ASN Wikibase Occurrence # 353697
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Date: | Friday 2 October 1998 |
Time: | 15:30 LT |
Type: | Beechcraft M35 |
Owner/operator: | Private |
Registration: | N9838R |
MSN: | D-6386 |
Total airframe hrs: | 3875 hours |
Engine model: | Continental IO-470-C |
Fatalities: | Fatalities: 0 / Occupants: 1 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Carter, OK -
United States of America
|
Phase: | En route |
Nature: | Private |
Departure airport: | Clinton, OK (KCLK) |
Destination airport: | |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The airplane impacted terrain following a forced landing resulting from a loss of engine power while in cruise flight. The airplane underwent 'extensive' modification and repair for five to six months prior to the flight. Several maintenance personnel, who were working on the airplane the morning of the accident, stated that the pilot wanted the airplane back, even though he was told that maintenance was not complete. Also, one maintenance person reported that the pilot said, 'no matter what, I'm pulling this airplane out and flying to Albuquerque.' After about 30 minutes of flight, the engine 'quit.' The left wing tank fuel quantity gauge indicated '3/4 full.' The pilot then switched the fuel tank selector switch from the left main wing tank to the right main wing tank and attempted to restart the engine, but was unsuccessful. He then tried to restart the engine with the auxiliary tank selected, but was unsuccessful. A forced landing was executed to a paved, country road. The airplane veered to the right into a ditch, subsequently the right wing dug into the ground and turned the airplane 180 degrees into a ditch.
Probable Cause: Fuel starvation. Factors were; the pilot's self induced pressure to fly the aircraft when maintenance had not been completed, poor judgement by the pilot to commence and continue flight with known deficiencies in the aircraft, and the lack of suitable terrain for a forced landing.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | FTW99LA003 |
Status: | Investigation completed |
Duration: | 2 years and 4 months |
Download report: | Final report |
|
Sources:
NTSB FTW99LA003
Location
Revision history:
Date/time | Contributor | Updates |
10-Mar-2024 09:32 |
ASN Update Bot |
Added |
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