Accident Cessna 414 C-GLHP,
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ASN Wikibase Occurrence # 353719
 
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Date:Monday 28 September 1998
Time:12:55 LT
Type:Silhouette image of generic C414 model; specific model in this crash may look slightly different    
Cessna 414
Owner/operator:Skyward Aviation
Registration: C-GLHP
MSN: 414-0099
Year of manufacture:1970
Total airframe hrs:5442 hours
Engine model:Continental TSIO 520-NB
Fatalities:Fatalities: 0 / Occupants: 5
Aircraft damage: Substantial
Category:Accident
Location:Burley, ID -   United States of America
Phase: Landing
Nature:Unknown
Departure airport:Billings, MT (KBIL)
Destination airport:
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
The flight crew reported that while taxiing after their first landing, the co-pilot reported to the captain that the left brake did not feel normal. The captain agreed and they taxied the aircraft to a maintenance facility for inspection. The mechanic visually inspected the brake system and did not find anything. The flight crew reported that the brake lines had recently been replaced and the mechanic instructed the flight crew to pump the brakes in case of air in the lines. The flight crew reported that they pumped the brakes prior to takeoff and felt that the pressure was now okay. The flight crew reported that during the second landing ground roll, the left braking action failed. The captain made a decision to apply hard right rudder and right brake to deliberately ground loop the aircraft before it ran off the end of the runway and into a river. The brake system was inspected and the left side brake master cylinder was removed for testing. During the functional test, it was found that the master cylinder assembly met all engineering requirements. The spot putty in place locking the cover to the body was consistent with Cessna production assembly practices which indicated that the cylinder had never been overhauled. The unit was disassembled and no evidence of wear, scratches or pitting were found.

Probable Cause: A brake system failure for undetermined reasons. An intentional ground loop was a factor.

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: SEA98LA178
Status: Investigation completed
Duration: 1 year and 3 months
Download report: Final report

Sources:

NTSB SEA98LA178

Location

Revision history:

Date/timeContributorUpdates
10-Mar-2024 09:51 ASN Update Bot Added

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