ASN Wikibase Occurrence # 353788
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Date: | Wednesday 16 September 1998 |
Time: | 17:30 LT |
Type: | Piper PA-24 |
Owner/operator: | Delta Romeo Corp. |
Registration: | N7003P |
MSN: | 24-2148 |
Year of manufacture: | 1960 |
Total airframe hrs: | 4403 hours |
Engine model: | Lycoming O-360-A1A |
Fatalities: | Fatalities: 0 / Occupants: 3 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Centre, AL -
United States of America
|
Phase: | Landing |
Nature: | Private |
Departure airport: | Atlanta, GA (KFTY) |
Destination airport: | (C22) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The pilot reported that he entered the traffic pattern but did not see the wind sock. He entered the traffic pattern to land on runway 27, and while on final approach, the airplane was high and fast. At the point he decided to go-around, he thought the airplane would be unable to clear trees ahead. He continued the approach and the airplane was landed about two-thirds down the 3,401 foot long runway. Unable to stop the airplane, it rolled off the end of the runway and collided with a ditch during which the left main landing gear collapsed. A weather observation taken about 25 minutes after the accident from an airport located 25 nautical miles and 240 degrees from the accident airport revealed in part that the wind was from 150 degrees at 4 knots. The pilot further reported that post accident he observed the wind sock and it was operational.
Probable Cause: The failure of the pilot to attain the proper touchdown point and his delay in initiating a go-around during a high and fast approach. A factor was the ditch.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | MIA98LA247 |
Status: | Investigation completed |
Duration: | 1 year and 6 months |
Download report: | Final report |
|
Sources:
NTSB MIA98LA247
Location
Revision history:
Date/time | Contributor | Updates |
10-Mar-2024 10:30 |
ASN Update Bot |
Added |
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