ASN Wikibase Occurrence # 353796
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Date: | Monday 14 September 1998 |
Time: | 15:10 LT |
Type: | Stinson 108-1 |
Owner/operator: | Private |
Registration: | N8666K |
MSN: | 108-1666 |
Total airframe hrs: | 1613 hours |
Engine model: | Lycoming O-360-A4A |
Fatalities: | Fatalities: 0 / Occupants: 1 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Spray, OR -
United States of America
|
Phase: | Unknown |
Nature: | Private |
Departure airport: | Kimberly, OR (OR49) |
Destination airport: | Spray, OR |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The pilot reported through counsel that on descent to his destination, he experienced a 'rough engine' and attempted a precautionary landing at a farm airport. He stated he 'misjudged [a] power line on approach' to the precautionary landing area, striking the power line and landing hard in a farm field. The pilot's report indicated no mechanical malfunction or failure was involved, expressing a belief that the power loss was due to carburetor icing. Temperature and dewpoint reported at the nearest weather observation station during the accident time frame did not indicate that a carburetor ice hazard existed. An FAA inspector who examined the wreckage the day after the accident found the airplane's fuel tanks nearly full of automotive or mixed automotive/aviation fuel; however, the pilot's accident report indicated the pilot did not know how much fuel was on board at the last takeoff. The pilot had not received a required biennial flight review in approximately 11 years, and he did not possess a current medical certificate. Additionally, the airplane had not received any inspections in the last 4 years.
Probable Cause: A partial loss of engine power, and the pilot's subsequent misjudgment of clearance with a transmission wire during a precautionary landing approach. The reason for the power loss was not determined; however, the pilot reported that it was not of a mechanical nature. The transmission wire was a factor.
Accident investigation:
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| |
Investigating agency: | NTSB |
Report number: | SEA98LA177 |
Status: | Investigation completed |
Duration: | 1 year and 3 months |
Download report: | Final report |
|
Sources:
NTSB SEA98LA177
Location
Revision history:
Date/time | Contributor | Updates |
10-Mar-2024 10:36 |
ASN Update Bot |
Added |
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