Accident Beechcraft D95A N924JL,
ASN logo
ASN Wikibase Occurrence # 353984
 
This information is added by users of ASN. Neither ASN nor the Flight Safety Foundation are responsible for the completeness or correctness of this information. If you feel this information is incomplete or incorrect, you can submit corrected information.

Date:Thursday 6 August 1998
Time:19:30 LT
Type:Silhouette image of generic BE95 model; specific model in this crash may look slightly different    
Beechcraft D95A
Owner/operator:Private
Registration: N924JL
MSN: TD-670
Total airframe hrs:4100 hours
Engine model:Lycoming IO-360-B1B
Fatalities:Fatalities: 0 / Occupants: 2
Aircraft damage: Substantial
Category:Accident
Location:Albuquerque, NM -   United States of America
Phase: Landing
Nature:Private
Departure airport:Santa Rosa, NM (Q58)
Destination airport:(KAEG)
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
The pilot reported that he was landing on runway 22, and during landing roll, the airplane pitched forward and to the right. According to the pilot's statement in the NTSB Pilot/Operator Aircraft Accident Report; 'On rollout, as aircraft started slowing down, I noticed the nose start to drop and the next thing I realized was the nose continued down, and then we were sliding along the runway with all the gear collapsed.' He said that the airplane exited the runway to the right and came to rest facing the opposite direction. Post-accident examination of the landing gear system revealed no mechanical anomalies which would have precluded normal operation. The right main inner gear door exhibited crushing and inward deformation. A representative from Beechcraft stated that when the landing gear is down and locked, the inner gear doors are up and locked (flush with the bottom of the airplane). He further stated that the landing gear handle and the flap handle in this airplane are reverse from the majority of general aviation aircraft. The pilot reported that he purchased the airplane on July 30, 1998, 7 days before the accident. He further indicated in the NTSB Report that he had a total of 15 hours of flight experience in the make & model aircraft.

Probable Cause: The pilot's inadvertent raising of the landing gear during landing rollout

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: FTW98LA375
Status: Investigation completed
Duration: 1 year and 5 months
Download report: Final report

Sources:

NTSB FTW98LA375

Location

Revision history:

Date/timeContributorUpdates
10-Mar-2024 17:43 ASN Update Bot Added

Corrections or additions? ... Edit this accident description

The Aviation Safety Network is an exclusive service provided by:
Quick Links:

CONNECT WITH US: FSF on social media FSF Facebook FSF Twitter FSF Youtube FSF LinkedIn FSF Instagram

©2024 Flight Safety Foundation

1920 Ballenger Av, 4th Fl.
Alexandria, Virginia 22314
www.FlightSafety.org