Serious incident McDonnell Douglas DC-9-51 N601AP,
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ASN Wikibase Occurrence # 354810
 
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Date:Monday 9 February 1998
Time:10:47 LT
Type:Silhouette image of generic DC95 model; specific model in this crash may look slightly different    
McDonnell Douglas DC-9-51
Owner/operator:Hawaiian Airlines
Registration: N601AP
MSN: 47658/790
Year of manufacture:1975
Total airframe hrs:43210 hours
Engine model:P&W JT8D-17
Fatalities:Fatalities: 0 / Occupants: 144
Aircraft damage: Minor
Category:Serious incident
Location:Honolulu, HI -   United States of America
Phase: Take off
Nature:Unknown
Departure airport:(KHNL)
Destination airport:Kona, HI (KOA)
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
During takeoff the crew heard a loud oscillating sound and aborted takeoff. The tower reported fire was visible from their right engine. The aircraft stopped and the crew initiated the engine fire and emergency evacuation check lists. The forward right service door was opened but the slide did not inflate. The airstairs were then deployed and the occupants deplaned. An inspection revealed an engine bearing cage had disintegrated. The evacuation slide was tested and functioned properly; however, its inflation bottle was found to be empty. While required, the bottle had not been checked that day because of a change in the operations manual that had resulted in confusion as to whose responsibility it was to perform the daily pressure checks. The manual states that it is the captain's responsibility to ensure that the bottle is pressurized but it is not an item on the preflight checklist. The flight crew thought maintenance personnel were performing the checks while maintenance personnel thought the crews were checking the bottles. The bottles have a history of sometimes losing pressure over time.

Probable Cause: the disintegration of the No. 6 bearing in the No. 2 engine which resulted in an aborted takeoff. In addition, the malfunction of the slide in the right forward service door was the result of a faulty seal in the inflation system. The inflation gauge had not been checked that day due to confusion resulting from a change in the operations manual. The change in the language made it unclear as to whose responsibility it was to check the inflation gauge. The operator did not verify that the change was being properly implemented after it had been made effective.

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: LAX98IA085
Status: Investigation completed
Duration: 3 years
Download report: Final report

Sources:

NTSB LAX98IA085

Location

Revision history:

Date/timeContributorUpdates
11-Mar-2024 18:32 ASN Update Bot Added

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