ASN Wikibase Occurrence # 354991
This information is added by users of ASN. Neither ASN nor the Flight Safety Foundation are responsible for the completeness or correctness of this information.
If you feel this information is incomplete or incorrect, you can
submit corrected information.
Date: | Tuesday 25 November 1997 |
Time: | 11:50 LT |
Type: | Piper PA-28-140 |
Owner/operator: | Private |
Registration: | N1816J |
MSN: | 2824245 |
Total airframe hrs: | 2753 hours |
Engine model: | Lycoming O-320-E2A |
Fatalities: | Fatalities: 0 / Occupants: 2 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Middlefield, OH -
United States of America
|
Phase: | Take off |
Nature: | Private |
Departure airport: | (7G8) |
Destination airport: | Mc Alpin, FL (FL10) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:During the initial climb after a normal takeoff, the airplane experienced a gradual loss of engine power. While turning to avoid some houses, the airplane struck power lines and impacted terrain. Examination of the log books revealed this was the airplane's first flight since an annual inspection had been completed. At that time, the airplane's carburetor was removed, disassembled and it's two piece venturi was replaced with a one piece venturi, per Precision Airmotive Service Bulletin # MSA-2. Also, the airplane had not been flown for over a month prior to the accident. On-scene examination of the airplane did not reveal any evidence of a preimpact failure of the airframe or engine. An engine run-up and a carburetor tear-down and flow check did not disclose any evidence of malfunction. Automotive gasoline was being used as fuel per a Supplemental Type Certificate. At an airport about 21 miles southeast of the accident site, the wind was reported to be from 200 degrees at 11 gusting 17 knots. The temperature and dew point were reported to be 34 and 23 degrees, respectively. According to icing probability charts, conditions were conducive to possible carburetor icing; however, carburetor icing was not verified. The pilot had checked the carburetor heat before takeoff, but did not report engaging it after the engine started losing power.
Probable Cause: loss of engine power for undetermined reasons.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | NYC98LA032 |
Status: | Investigation completed |
Duration: | 1 year |
Download report: | Final report |
|
Sources:
NTSB NYC98LA032
Location
Revision history:
Date/time | Contributor | Updates |
12-Mar-2024 06:50 |
ASN Update Bot |
Added |
The Aviation Safety Network is an exclusive service provided by:
CONNECT WITH US:
©2024 Flight Safety Foundation