ASN Wikibase Occurrence # 355027
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Date: | Monday 17 November 1997 |
Time: | 11:30 LT |
Type: | Cessna 172G |
Owner/operator: | Private |
Registration: | N202EX |
MSN: | 17253456 |
Total airframe hrs: | 3000 hours |
Engine model: | Continental O-300-D |
Fatalities: | Fatalities: 0 / Occupants: 2 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Van, TX -
United States of America
|
Phase: | Initial climb |
Nature: | Unknown |
Departure airport: | |
Destination airport: | |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The airplane impacted terrain during a forced landing following a total loss of engine power. The pilot reported that this was the first 'test' flight, following repair and re-assembly of the airplane, since its previous accident, which occurred on 5/9/96. The pilot stated that he took off from runway 04, and during the initial climb-out phase at about 150 feet AGL, a complete loss of engine power occurred. The pilot reported that he 'pumped' the throttle, and there was a 'momentary burst' of power. The pilot stated that he continued to pump the throttle, but this did not yield further results. The pilot then executed a forced landing. The pilot banked the airplane to the left, and it contacted power lines. The airplane then impacted the ground, turned 180 degrees, and came to rest upright, adjacent to a line of trees. Examination of the carburetor revealed that the float valve retractor clip was improperly installed, which restricted float travel. The float drop was improperly set at 1.5 inches. The proper setting was between 1.72 to 1.78 inches. The restricted float travel resulted in fuel starvation to the engine and subsequent loss of engine power.
Probable Cause: fuel starvation, resulting from restricted carburetor float travel, due to improper maintenance installation. The encounter with a power line was related factor.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | FTW98LA050 |
Status: | Investigation completed |
Duration: | 8 months |
Download report: | Final report |
|
Sources:
NTSB FTW98LA050
History of this aircraft
Other occurrences involving this aircraft Location
Revision history:
Date/time | Contributor | Updates |
12-Mar-2024 07:10 |
ASN Update Bot |
Added |
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