ASN Wikibase Occurrence # 355047
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Date: | Friday 7 November 1997 |
Time: | 18:30 LT |
Type: | Beechcraft C23 |
Owner/operator: | Air Accord |
Registration: | N3724Z |
MSN: | M-2281 |
Total airframe hrs: | 2667 hours |
Engine model: | Lycoming O-360 |
Fatalities: | Fatalities: 0 / Occupants: 4 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Corona, CA -
United States of America
|
Phase: | Landing |
Nature: | Private |
Departure airport: | Bakersfield, CA (KBFL) |
Destination airport: | San Diego, CA (KSEE) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The pilot reported that he had full fuel onboard. About 1 hour into the flight, the pilot descended and switched the fuel selector to the right tank. The engine ran rough and was 'hesitant.' When he switched back to the left tank, the engine ran normally. He elected to make a precautionary landing at a nearby airport. During his descent he switched back to the right tank and the engine ran rough again. He was not able to receive a traffic advisory and was unable to see the windsock. On final approach he realized he had a tail wind and was too high and fast. He initiated a go-around but the engine was sluggish and the airplane would not climb. The pilot headed for an open field to make an off-airport emergency landing and the engine quit. The airplane brushed the tops of some trees and touched down in the field. The nose gear struck a rock during the landing roll and the nose gear collapsed. The engine was test run following recovery and operated for about 5 minutes through the full range of operation with and without the electric fuel pump, on both fuel tanks. About 5.6 gallons of fuel were drained from the left tank and 17.9 gallons were drained from the right tank. No debris, water, or restrictions were noted in the fuel lines, carburetor bowl, or fuel strainer.
Probable Cause: The loss of engine power for undetermined reasons. A factor was the rough terrain that resulted in a nose over during the landing roll.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | LAX98LA035 |
Status: | Investigation completed |
Duration: | 1 year and 7 months |
Download report: | Final report |
|
Sources:
NTSB LAX98LA035
History of this aircraft
Other occurrences involving this aircraft Revision history:
Date/time | Contributor | Updates |
12-Mar-2024 07:22 |
ASN Update Bot |
Added |
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