Fuel exhaustion Accident Mooney M20C N1360W,
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ASN Wikibase Occurrence # 355059
 
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Date:Monday 3 November 1997
Time:14:35 LT
Type:Silhouette image of generic M20P model; specific model in this crash may look slightly different    
Mooney M20C
Owner/operator:Private
Registration: N1360W
MSN: 2641
Total airframe hrs:3253 hours
Engine model:Lycoming O-360-A1D
Fatalities:Fatalities: 0 / Occupants: 1
Aircraft damage: Substantial
Category:Accident
Location:Ozona, TX -   United States of America
Phase: En route
Nature:Private
Departure airport:Mckinney, TX (TX05)
Destination airport:(KOZA)
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
During a return flight from McKinney to Ozona, TX, the aircraft's engine lost power due to fuel exhaustion. The pilot had flown the aircraft for 2.4 hours on the flight from Ozona to McKinney on the day before the accident. On the day of the accident, the pilot found that there was no fuel available at the departure airport, therefore he had planned a fuel stop at Abilene, TX. During cruise flight and 'after not encountering anticipated quartering head winds,' the pilot calculated that the time of flight direct to Ozona would be 2.5 hours. He then made the decision to 'continue direct to Ozona.' Approximately 20 miles northeast of Ozona, the engine lost power. The pilot initiated a forced landing to a pasture, and during the landing roll, the wings impacted some 'scrubby' trees. The pilot reported to an FAA inspector that he had 'run out of fuel.' The pilot also reported that he had flown the same route of flight before without refueling; however, the airplane's engine had been changed, and he had not anticipated the higher fuel burn rate.

Probable Cause: the pilot's improper planning/decision, which led to fuel exhaustion, loss of engine power, and a forced landing. A related factor was the lack of suitable terrain for the forced landing.

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: FTW98LA042
Status: Investigation completed
Duration: 12 months
Download report: Final report

Sources:

NTSB FTW98LA042

Location

Revision history:

Date/timeContributorUpdates
12-Mar-2024 07:29 ASN Update Bot Added

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