Accident Piper PA-23-250 N40201,
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ASN Wikibase Occurrence # 355066
 
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Date:Saturday 1 November 1997
Time:12:19 LT
Type:Silhouette image of generic PA27 model; specific model in this crash may look slightly different    
Piper PA-23-250
Owner/operator:Private
Registration: N40201
MSN: 27-7304998
Year of manufacture:1973
Engine model:Lycoming TIO-540-C1A
Fatalities:Fatalities: 0 / Occupants: 1
Aircraft damage: Substantial
Category:Accident
Location:Galveston, TX -   United States of America
Phase: Initial climb
Nature:Ferry/positioning
Departure airport:(KGLS)
Destination airport:Colorado Sprgs, CO
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
After takeoff, at about 250 to 300 feet AGL, the right engine lost partial power, followed by the left engine. The pilot made a wide left turn toward a small field with trees in front, and retracted the landing gear. During the forced landing, the pilot 'intentionally' hit the trees in order to slow down and go under some power lines. After going under the wires, the airplane came to a stop in the field. The airplane had not been flown for about two years, and the pilot was to ferry the aircraft for the owner from Galveston, TX, to Colorado Springs, CO. A mechanic at the Scholes Field Airport in Galveston prepared the airplane for the flight and obtained a ferry permit from the FAA. The mechanic reported that the fuel tanks were drained and visually inspected. About one gallon of water was drained from the tanks, and both fuel filters were cleaned. The mechanic also reported that rained had fallen on the day before the accident flight. Examination of the fuel filters revealed that they were both clogged with debris.

Probable Cause: inadequate maintenance and/or preflight inspection of the airplane, and subsequent blockage of the fuel filters, which led to fuel starvation, partial loss of engine power in both engines, and a forced landing. A related factor was the lack of suitable terrain for the forced landing.

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: FTW98LA038
Status: Investigation completed
Duration: 12 months
Download report: Final report

Sources:

NTSB FTW98LA038

Location

Revision history:

Date/timeContributorUpdates
12-Mar-2024 07:35 ASN Update Bot Added

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