ASN Wikibase Occurrence # 355168
This information is added by users of ASN. Neither ASN nor the Flight Safety Foundation are responsible for the completeness or correctness of this information.
If you feel this information is incomplete or incorrect, you can
submit corrected information.
Date: | Saturday 4 October 1997 |
Time: | 08:10 LT |
Type: | Boeing 737-200 |
Owner/operator: | Southwest Airlines |
Registration: | N129SW |
MSN: | 22340/678 |
Year of manufacture: | 1980 |
Total airframe hrs: | 49400 hours |
Engine model: | P&W JT8D-9 |
Fatalities: | Fatalities: 0 / Occupants: 50 |
Aircraft damage: | Minor |
Category: | Serious incident |
Location: | Chicago, IL -
United States of America
|
Phase: | Landing |
Nature: | Unknown |
Departure airport: | Kansas City, MO (KMCI) |
Destination airport: | (KMDW) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The left main landing gear outboard wheel/brake assembly separated from the airplane during a landing roll. The Captain did not report any difficulties in controlling the airplane. Inspection of the failed axle revealed a crack which originated at the surface of one of the brake flange holes. This crack had previously been repaired. Detailed metallurgical examination of the crack revealed properties consistent with the surface having been heated to an excessive temperature during the repair process.
Probable Cause: an improper repair to a crack in a brake flange hole on the left main landing gear outboard axle, and subsequent fatigue failure of the axle.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | CHI98IA007 |
Status: | Investigation completed |
Duration: | 1 year |
Download report: | Final report |
|
Sources:
NTSB CHI98IA007
Location
Revision history:
Date/time | Contributor | Updates |
12-Mar-2024 09:04 |
ASN Update Bot |
Added |
The Aviation Safety Network is an exclusive service provided by:
CONNECT WITH US:
©2024 Flight Safety Foundation