Accident Piper PA-32R-301 N8147B,
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ASN Wikibase Occurrence # 355380
 
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Date:Saturday 16 August 1997
Time:19:09 LT
Type:Silhouette image of generic P32R model; specific model in this crash may look slightly different    
Piper PA-32R-301
Owner/operator:Jefferson City Flying Service
Registration: N8147B
MSN: 32R-8013048
Total airframe hrs:7125 hours
Engine model:Lycoming IO-540-K1G5D
Fatalities:Fatalities: 0 / Occupants: 4
Aircraft damage: Substantial
Category:Accident
Location:Jefferson City, MO -   United States of America
Phase: Initial climb
Nature:Private
Departure airport:(KJEF)
Destination airport:
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
The pilot said that they had just taken off and were 'approximately 20 to 25 feet in the air when the engine rpm dropped from 2,700 to 400.' As the airspeed decreased, the airplane began to roll to the left. The pilot said that he kept the nose of the airplane up, and leveled the wings. 'As the airplane began to settle, the rpm zoomed to 700. The airplane touched down and then bounced back into the air.' The airplane was about 20 feet above the ground when the rpm dropped to zero and the left wing dropped again. The pilot again leveled the wings. By this time the airplane was left of the runway. The pilot decided to land in the dirt along-side the runway. 'The airplane touched down hard and then slid for a short distance.' The passenger in the right front seat said that after a short takeoff roll, the airplane got airborne, came down, bounced back in the air, and then came down very fast hitting left wing first. The passenger in the right rear seat said that it was loud when they took off and that the airplane was vibrating and seemed very rough. Examination of the airplane's stabilizer trim showed an almost full nose up trim setting. The rudder trim was set at full nose left. No other anomalies were revealed with the airplane.

Probable Cause: the pilot's incomplete preflight of the airplane's stabilizer and rudder trim settings for takeoff, his failure to correct for the high pitch during the initial climb, his failure to recover from the bounced landing, and the inadvertent stall. Factors relating to this accident were the improper stabilizer and rudder trim settings.

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: CHI97LA262
Status: Investigation completed
Duration: 4 months
Download report: Final report

Sources:

NTSB CHI97LA262

Location

Revision history:

Date/timeContributorUpdates
12-Mar-2024 11:24 ASN Update Bot Added

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