Accident WACO Classic Aircraft YMF-5 N14128,
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ASN Wikibase Occurrence # 355483
 
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Date:Monday 28 July 1997
Time:16:40 LT
Type:Silhouette image of generic WACF model; specific model in this crash may look slightly different    
WACO Classic Aircraft YMF-5
Owner/operator:Reilly Aviation
Registration: N14128
MSN: 4213
Year of manufacture:1934
Total airframe hrs:4045 hours
Engine model:Jacobs R-755-9
Fatalities:Fatalities: 0 / Occupants: 3
Aircraft damage: Substantial
Category:Accident
Location:Lake Buena Vist, FL -   United States of America
Phase: En route
Nature:Unknown
Departure airport:Kissimmee, FL (KISM)
Destination airport:
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
During cruise flight, the pilot noted an engine vibration followed by a total loss of engine power. He made a forced landing, but was unable to reach suitable terrain. During the landing rollout, he observed a ditch and intentionally ground looped the airplane, but the airplane collided with a pole. Examination of the propeller revealed the propeller retention nut was hand tight. Galling was present on the propeller hub mounting flange and the rear cone. Disassembly of the engine assembly revealed the crankshaft was broken at the counterweight flange. Visual inspection of the shear surfaces on the crankcase showed tell tale benchmarks that appeared to have originated at the oil way plug threads and progressed through approximately one fifth of the crank circumference. Interviews with personnel involved with the installation revealed they had retorqued the propeller, but had not followed accepted industry practices in establishing proper hub to rear cone contact surfaces.

Probable Cause: failure of maintenance personnel to follow installation procedures pertaining to the torque of the propeller retention nut, which resulted in a loose propeller retention nut, subsequent fatigue failure of the crankshaft, and loss of engine power. The lack of suitable terrain for an emergency landing was a related factor.

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: MIA97LA222
Status: Investigation completed
Duration: 10 months
Download report: Final report

Sources:

NTSB MIA97LA222

Location

Revision history:

Date/timeContributorUpdates
12-Mar-2024 12:28 ASN Update Bot Added

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