ASN Wikibase Occurrence # 355506
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Date: | Friday 25 July 1997 |
Time: | 09:45 LT |
Type: | Cessna 150D |
Owner/operator: | Private |
Registration: | N4228U |
MSN: | 15060228 |
Year of manufacture: | 1963 |
Total airframe hrs: | 3156 hours |
Engine model: | Continental O-200A |
Fatalities: | Fatalities: 0 / Occupants: 2 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Fort Collins, CO -
United States of America
|
Phase: | Initial climb |
Nature: | Private |
Departure airport: | (3V5) |
Destination airport: | Osage, IA (D02) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:During initial climb following takeoff on a cross-country flight, the aircraft failed to attain a sustained climb and impacted in a field approximately 2 miles from the departure end of the runway. Weather conditions at the time were temperature 92 degrees F, wind calm, and the airport elevation was 4,699 feet msl. The aircraft had been modified by STC to a tailwheel configuration. The Owner's Manual in the aircraft was for the wrong year and model. The aircraft was 32 pounds over maximum gross weight. The pilot was using 10 degrees flaps for takeoff. There are no performance charts for the use of flaps for takeoff and in the narrative portion of the Owner's Manual. The manual recommends that flaps not be used for takeoff from high altitude airports on hot days. In addition, the aircraft was out of annual, the pilot had a forged medical certificate, some work on the aircraft had been performed by the pilot and signed off and he did not possess a mechanic license, and the signatures on the spark plugs revealed the aircraft engine was not leaned for optimum performance.
Probable Cause: Inadequate preflight planning by loading the aircraft over the maximum certificated gross weight, failure to follow procedures and directives by using flaps for takeoff and failing to properly lean the engine for optimum power, and stalling the aircraft. Factors were: Poor judgement by the pilot in operating the aircraft without a current annual inspection, for forging his medical certificate, and failing to obtain and use the proper Owner's Manual for the aircraft. Also, factors were insufficient requirements for the Owner's Manual by the FAA and inadequate aircraft manual information by the manufacturer.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | FTW97FA280 |
Status: | Investigation completed |
Duration: | 1 year and 3 months |
Download report: | Final report |
|
Sources:
NTSB FTW97FA280
Location
Revision history:
Date/time | Contributor | Updates |
12-Mar-2024 12:41 |
ASN Update Bot |
Added |
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