Accident Cessna 310R N502SB,
ASN logo
ASN Wikibase Occurrence # 35575
 
This information is added by users of ASN. Neither ASN nor the Flight Safety Foundation are responsible for the completeness or correctness of this information. If you feel this information is incomplete or incorrect, you can submit corrected information.

Date:Saturday 3 September 1994
Time:02:10 LT
Type:Silhouette image of generic C310 model; specific model in this crash may look slightly different    
Cessna 310R
Owner/operator:Smithkline Beecham Bio Labs
Registration: N502SB
MSN: 310R0244
Total airframe hrs:10508 hours
Engine model:CONTINENTAL IO-520-M1
Fatalities:Fatalities: 2 / Occupants: 2
Aircraft damage: Destroyed
Category:Accident
Location:Blain, PA -   United States of America
Phase: Unknown
Nature:Executive
Departure airport:West Mifflin, PA (AGC
Destination airport:Pottstown, PA (PTW
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
THE AIRPLANE WAS IN A CRUISE DESCENT FROM 9000 TO 7000 FEET AT NIGHT IN VISUAL METEOROLOGICAL CONDITIONS, WHEN, ACCORDING TO RECORDED RADAR DATA, THE ALTITUDE INCREASED 200 FEET AND THEN RADAR CONTACT WAS LOST AT 7800 FEET. WITNESSES SAW THE AIRPLANE IN A STEEP DESCENT AND HEARD A LOUD WHINE. THE AIRPLANE SUSTAINED INFLIGHT AIRFRAME SEPARATION. DEBRIS WAS SCATTERED OVER A DISTANCE OF ABOUT 1500 FT WITH THE HORIZONTAL STABILIZERS AND ELEVATORS FOUND NEAR THE BEGINNING OF THE WRECKAGE PATH, FOLLOWED BY THE FUSELAGE, AND ENDING WITH THE ENGINES AND PROPELLERS. THE LEFT HORIZONTAL STABILIZER HAD FAILED DOWN AND AFT. THE LEFT WING OUTBOARD OF THE LEFT ENGINE HAD FAILED DOWN AND WAS FOUND 600 FT LEFT OF THE DEBRIS TRAIL. WRINKLES IN TWO DIRECTIONS AND POPPED RIVETS WERE FOUND ON BOTH WINGS. TOXICOLOGY TESTS OF THE PILOT'S BLOOD REVEALED 0.002 UG/ML OF TETRAHYDROCANNABINOL (MARIJUANA) AND 0.011 UG/ML TETRAHYDROCANNABINOL CARBOXYLIC ACID. A TEST OF HIS URINE SHOWED 0.305 UG/ML OF TETRAHYDROCANNABINOL CARBOXYLIC ACID. THE PILOT HAD WORKED A FULL-TIME CONSTRUCTION JOB DURING THE DAY, AND HE HAD BEEN AWAKE FOR ABOUT 19 HOURS.

Probable Cause: THE PILOT'S IMPAIRMENT OF JUDGMENT AND PERFORMANCE DUE TO DRUGS, FAILURE TO MAINTAIN CONTROL OF THE AIRPLANE, AND EXCEEDING THE DESIGN STRESS LIMITS OF THE AIRPLANE, WHICH RESULTED IN AN IN-FLIGHT BREAKUP OF THE AIRPLANE. A FACTOR RELATED TO THE ACCIDENT WAS: CONDITIONS CONDUCIVE TO FATIGUE.

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: NYC94FA166
Status: Investigation completed
Duration: 12 months
Download report: Final report

Sources:

NTSB NYC94FA166

Location

Revision history:

Date/timeContributorUpdates
24-Oct-2008 10:30 ASN archive Added
21-Dec-2016 19:22 ASN Update Bot Updated [Time, Damage, Category, Investigating agency]
09-Apr-2024 19:30 ASN Update Bot Updated [Time, Other fatalities, Phase, Departure airport, Destination airport, Source, Narrative, Category, Accident report]

Corrections or additions? ... Edit this accident description

The Aviation Safety Network is an exclusive service provided by:
Quick Links:

CONNECT WITH US: FSF on social media FSF Facebook FSF Twitter FSF Youtube FSF LinkedIn FSF Instagram

©2024 Flight Safety Foundation

1920 Ballenger Av, 4th Fl.
Alexandria, Virginia 22314
www.FlightSafety.org