ASN Wikibase Occurrence # 355779
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Date: | Sunday 8 June 1997 |
Time: | 12:50 LT |
Type: | Cessna 150K |
Owner/operator: | Private |
Registration: | N6218G |
MSN: | 15071718 |
Year of manufacture: | 1970 |
Engine model: | Continental O-200-A |
Fatalities: | Fatalities: 0 / Occupants: 1 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Jay, ME -
United States of America
|
Phase: | En route |
Nature: | Private |
Departure airport: | Schenectady, NY (SCH |
Destination airport: | Pittsfield, ME (2B7) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The pilot was in cruise flight at 7,500 feet with the mixture leaned out when he developed 'engine problems.' The pilot thought he had encountered carburetor icing, so he applied carburetor heat and changed the mixture. The pilot was near Lebanon, New Hampshire, when it appeared the engine problem was resolved, so he chose to continue to his destination. The pilot reported that some time later, he heard a loud noise from under the engine and experienced engine 'roughness.' He pilot attempted to restore engine power by leaning the mixture, checking the magnetos, and by changing flight attitude and direction. However, after a few minutes the engine completely lost power. The pilot stated the engine stopped and he performed a forced landing to a road. During the forced landing, the airplane struck a sign, went over an embankment, and came to rest in a ditch. The pilot reported that he had been flying for 3 to 3.5 hours and that he should have had 5 hours of flight time on full tanks and that, '...fuel usage was 5 gallons per hour.' Examination of the wreckage revealed 1.5 gallons of fuel on board. According to the Pilot's Operating Handbook, the airplane had a 26 gallon fuel capacity, of which 22.5 gallons was usable. The duration of the accident flight was 3.8 hours.
Probable Cause: the pilot's inaccurate fuel consumption calculations which resulted in fuel exhaustion.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | NYC97LA111 |
Status: | Investigation completed |
Duration: | 10 months |
Download report: | Final report |
|
Sources:
NTSB NYC97LA111
Revision history:
Date/time | Contributor | Updates |
12-Mar-2024 15:32 |
ASN Update Bot |
Added |
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