ASN Wikibase Occurrence # 355964
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Date: | Saturday 26 April 1997 |
Time: | 12:30 LT |
Type: | Cessna 152 |
Owner/operator: | Morcom Aviation Services, Inc. |
Registration: | N152TM |
MSN: | 15279838 |
Year of manufacture: | 1977 |
Total airframe hrs: | 7113 hours |
Engine model: | Lycoming O-235-L2C |
Fatalities: | Fatalities: 0 / Occupants: 1 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Ilwaco, WA -
United States of America
|
Phase: | Landing |
Nature: | Training |
Departure airport: | Hillsboro, OR (KHIO) |
Destination airport: | Everett, WA (KPAE) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The student pilot departed on a solo cross-country flight during which deteriorating weather was forecast along the route. After the first leg of the flight, the pilot rested and did some additional flight planning, and then departed on the return leg. After departing an intermediate stop on the return leg of the flight, the pilot encountered rain, low clouds and high winds. He then elected to return to the airport where he had made the intermediate stop, but upon returning to that area, he found that he was unable to see the airport through the rain and clouds. While trying to fly to another airport, he happened to overfly a 2,000 foot runway, and elected to attempt a landing there. While on final approach to land, the rain, clouds, and crosswinds were significant enough that the pilot was having a hard time seeing the runway. He ultimately touched down past the mid-point of the runway, and the aircraft skidded off the end before he was able to get it stopped. When it departed the runway, the nose gear encountered soft terrain and was torn from the aircraft. It was later determined that the student's instructor did not monitor the preflight weather briefing and that the student did not get an updated weather briefing after his initial departure.
Probable Cause: The student pilot's failure to land the aircraft at the proper touchdown point. Factors include inadequate preflight planning/preparation by the student pilot, inadequate supervision by the student pilot's flight instructor, rain, fog, strong crosswinds, a wet runway, and soft terrain off the end of the runway,
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | SEA97LA092 |
Status: | Investigation completed |
Duration: | 12 months |
Download report: | Final report |
|
Sources:
NTSB SEA97LA092
History of this aircraft
Other occurrences involving this aircraft
2 July 1991 |
N757MA |
Kennewick Aircraft Serv. |
0 |
Richland, WA |
|
sub |
Location
Revision history:
Date/time | Contributor | Updates |
12-Mar-2024 17:37 |
ASN Update Bot |
Added |
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