ASN Wikibase Occurrence # 356520
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Date: | Friday 1 November 1996 |
Time: | 13:00 LT |
Type: | Yakovlev Yak-52 |
Owner/operator: | Biggles Aviation, Inc |
Registration: | N207YK |
MSN: | 9611913 |
Year of manufacture: | 1996 |
Total airframe hrs: | 5 hours |
Engine model: | Vendeneyev M14P |
Fatalities: | Fatalities: 0 / Occupants: 1 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Fullerton, CA -
United States of America
|
Phase: | Initial climb |
Nature: | Unknown |
Departure airport: | , CA (KFUL) |
Destination airport: | |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The aircraft was a new production airplane, which was manufactured in Romania, then was disassembled and shipped in a crate to the United States. This was the first flight following reassembly of the aircraft. The aircraft had been run on the ground for 50 minutes, and a high speed taxi test had been completed. Shortly after takeoff, a loss of engine power occurred. The pilot landed on the runway, but insufficient runway was remaining to stop before colliding with a building and a fence at the departure end of the runway. The powerplant was a Russian manufactured 9-cylinder radial engine with a pressure carburetor. The pilot said he believed that the carburetor malfunctioned. The aircraft was examined by an FAA airworthiness inspector with the assistance of a Russian factory trained technician. The carburetor was removed from the engine and a used/serviceable one was installed in its place. The engine was then started and exercised through the normal power range with no problem noted. The technician stated that disassembly of the carburetor required special tools available only at the factory. The inspector reported that the directions for disassembling the aircraft were used as a checklist/reference for reassembling the aircraft, and that the directions were written only in Russian. The Russian technician said that '. . . the factory did not do one or two steps on the checklist.'
Probable Cause: loss of engine power due to an undetermined internal carburetor malfunction. A factor relating to the accident was: the directions that were use for reassembly of the aircraft were written only in Russian.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | LAX97LA035 |
Status: | Investigation completed |
Duration: | 9 months |
Download report: | Final report |
|
Sources:
NTSB LAX97LA035
Revision history:
Date/time | Contributor | Updates |
13-Mar-2024 08:06 |
ASN Update Bot |
Added |
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