ASN Wikibase Occurrence # 356528
This information is added by users of ASN. Neither ASN nor the Flight Safety Foundation are responsible for the completeness or correctness of this information.
If you feel this information is incomplete or incorrect, you can
submit corrected information.
Date: | Tuesday 29 October 1996 |
Time: | 08:37 LT |
Type: | RotorWay Exec 162F |
Owner/operator: | Private |
Registration: | N711KN |
MSN: | 6072 |
Total airframe hrs: | 40 hours |
Engine model: | Rotorway 162F |
Fatalities: | Fatalities: 0 / Occupants: 1 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Haines, AK -
United States of America
|
Phase: | En route |
Nature: | Training |
Departure airport: | , AK (KHNS) |
Destination airport: | Juneau, AK (JNU) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The certificated private airplane pilot, the sole occupant & holder of a solo endorsement for helicopters, was beginning a cross-country flight in an experimental homebuilt helicopter. After takeoff, he heard a sharp bang & observed smoke in the cockpit. He declared an emergency, entered an autorotation, & selected an emergency landing area on a beach, but the area was covered with large boulders. During the flare & landing, the engine responded momentarily, when the pilot raised the collective pitch control, but the engine did not have sufficient power to hover. The helicopter sustained damage to the landing gear skids, the tail rotor, & the tail boom structure adjacent to the tail rotor assembly. An exam revealed the engine compartment was coated with engine coolant. The air intake filter was saturated with coolant, & 1 electronic ignition system was rendered inoperative from coolant saturation. A pressure test of the coolant system revealed a leak & spraying of coolant from a coolant pump manifold fitting. The pilot indicated the fitting had a rubber hose attached by a clamp, & coolant was leaking at the attach point. Also, he said the hose had been installed with excessive tension at the fitting due to it being 1/2 inch too short. He had accrued 47 hrs in helicopters.
Probable Cause: a leaking coolant hose that saturated the induction air filter and one electronic ignition system with coolant. Unsuitable terrain for a forced landing was a related factor in the accident.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | ANC97LA005 |
Status: | Investigation completed |
Duration: | 1 year and 5 months |
Download report: | Final report |
|
Sources:
NTSB ANC97LA005
Location
Revision history:
Date/time | Contributor | Updates |
13-Mar-2024 08:07 |
ASN Update Bot |
Added |
The Aviation Safety Network is an exclusive service provided by:
CONNECT WITH US:
©2024 Flight Safety Foundation