ASN Wikibase Occurrence # 356537
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Date: | Friday 25 October 1996 |
Time: | 17:15 LT |
Type: | Mooney M20K |
Owner/operator: | Private |
Registration: | N32DG |
MSN: | 25-1128 |
Year of manufacture: | 1987 |
Total airframe hrs: | 1544 hours |
Engine model: | Continental IO-360-MB1 |
Fatalities: | Fatalities: 0 / Occupants: 4 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Amelia Island, FL -
United States of America
|
Phase: | En route |
Nature: | Private |
Departure airport: | (55J) |
Destination airport: | Kissimmee, FL (KISM) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:During the climb after takeoff, the engine began to run rough, then lost power. According to the pilot, he turned on the boost pump, and the engine quit. The pump was turned off, the engine surged, then quit again. During a forced landing, the airplane struck trees, then came to rest on a street. Postaccident examination of the engine revealed corrosion in the left magneto, which was indicative of moisture contamination of the magneto that may have resulted in a loss of power. Additionally, the engine driven fuel pump pressure was set high, which would have resulted in a rich mixture, when the boost pump was activated. The engine had been equipped with pressure type, Slick Electro Model 6224 magnetos. A service bulletin, applicable to another aircraft manufacturer, had been issued by the magneto manufacturer to inspect the pressurized magnetos each 100 hours for evidence of moisture contamination. The same information was contained in the magneto maintenance and overhaul manual. The airplane was maintained under an annual inspection program, with no intervening 100 hour inspections; 159 hours of flight time had been accumulated since the last annual inspection.
Probable Cause: inadequate maintenance/inspection, which resulted in a failure to detect and correct moisture contamination of the left magneto; and/or improper adjustment of the engine fuel pump output, which resulted in excessive fuel pressure.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | ATL97LA009 |
Status: | Investigation completed |
Duration: | 10 months |
Download report: | Final report |
|
Sources:
NTSB ATL97LA009
Location
Revision history:
Date/time | Contributor | Updates |
13-Mar-2024 08:13 |
ASN Update Bot |
Added |
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