ASN Wikibase Occurrence # 356662
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Date: | Saturday 21 September 1996 |
Time: | 14:25 LT |
Type: | Bell 407 |
Owner/operator: | Bell Helicopter Textron Inc. |
Registration: | N1114S |
MSN: | 53043 |
Total airframe hrs: | 22 hours |
Engine model: | Allison 250C47B |
Fatalities: | Fatalities: 0 / Occupants: 3 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Kerrville, TX -
United States of America
|
Phase: | Approach |
Nature: | Unknown |
Departure airport: | (KERV) |
Destination airport: | |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:During the day prior to the accident, when the flight was 20 minutes from Kerrville after flying through a light rain, the RESTART FAULT light illuminated on the caution and warning light panel. The flight continued to Kerrville and landed without further incident. Maintenance was performed to correct the deficiencies. On the day of the accident, the helicopter's engine was started and ground run two times with all systems normal. A 10 minute test flight was performed and no discrepancies were noted. During the approach to Kerrville Airport, at 300 feet AGL, in a right turn, approximately 60 knots, the pilot noted the FADEC FAIL light and warning horn. During the autorotation, to avoid trees and houses, he extended the glide by increasing collective pitch. After clearing the obstacles, he leveled the helicopter and 'used all remaining collective for landing.' The helicopter 'landed hard and remained upright.' The pilot did not perform the emergency procedure for a FADEC FAIL warning light as prescribed by the Bell 407 Rotorcraft Flight Manual. An examination of the HMU harness revealed a manufacturing defect.
Probable Cause: The loss of power due to the pilot's failure to comply with established procedures. Factors were a short in the FADEC wiring harness due to a manufacturing defect, and the lack of suitable terrain for the forced landing.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | FTW96LA395 |
Status: | Investigation completed |
Duration: | 11 months |
Download report: | Final report |
|
Sources:
NTSB FTW96LA395
Location
Revision history:
Date/time | Contributor | Updates |
13-Mar-2024 09:37 |
ASN Update Bot |
Added |
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