ASN Wikibase Occurrence # 357105
This information is added by users of ASN. Neither ASN nor the Flight Safety Foundation are responsible for the completeness or correctness of this information.
If you feel this information is incomplete or incorrect, you can
submit corrected information.
Date: | Saturday 6 July 1996 |
Time: | 15:40 LT |
Type: | Hughes 369D |
Owner/operator: | Evergreen Helicopters Inc. |
Registration: | N5110Y |
MSN: | 510970D |
Total airframe hrs: | 6013 hours |
Engine model: | Allison 250-C20B |
Fatalities: | Fatalities: 0 / Occupants: 2 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Mcminnville, OR -
United States of America
|
Phase: | Manoeuvring (airshow, firefighting, ag.ops.) |
Nature: | Unknown |
Departure airport: | , OR (KMMV) |
Destination airport: | |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The engine fuel governor had been replaced since the previous flight. About 4 minutes after takeoff, while maneuvering at 400 to 500 feet above ground level, the helicopter's Engine Power Out (EPO) warning light and horn activated. The pilot reduced collective and entered an autorotation, but had to turn downwind to clear trees. The engine N2 (power turbine) RPM was stabilized at 88 to 90 percent during the descent, as compared to a normal range of 102 to 103 percent. The helicopter touched down in a soft field at 20 to 25 MPH forward speed, slid about 30 feet, and rolled over. On-site investigators found the adjustable governor lever control rod disconnected from the governor control lever, which a McDonnell Douglas investigator stated would result in loss of automatic governing of engine RPM. The nut and washer for securing the adjustable control rod to the governor control lever were found in the bottom of the engine compartment, but the cotter pin specified for safetying the nut and washer was not located. The aircraft operating handbook directed pilots to check the fuel control and N2 governor linkages during preflight inspection.
Probable Cause: improper maintenance (replacement) and inspection of the engine fuel governor by company maintenance personnel, the pilot's inadequate preflight inspection, and a subsequent disconnect of the adjustable governor lever control rod, which disabled the engine speed governor and resulted in a partial loss of engine power. Factors relating to the accident were: trees and soft terrain in the emergency landing area, and a tailwind during the forced landing touchdown.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | SEA96LA144 |
Status: | Investigation completed |
Duration: | 1 year 1 month |
Download report: | Final report |
|
Sources:
NTSB SEA96LA144
Location
Revision history:
Date/time | Contributor | Updates |
13-Mar-2024 14:17 |
ASN Update Bot |
Added |
The Aviation Safety Network is an exclusive service provided by:
CONNECT WITH US:
©2024 Flight Safety Foundation