ASN Wikibase Occurrence # 357137
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Date: | Tuesday 2 July 1996 |
Time: | 08:30 LT |
Type: | Piper PA-31-310 Navajo |
Owner/operator: | Satellite Aero Inc. |
Registration: | N27518 |
MSN: | 31-7812038 |
Total airframe hrs: | 7726 hours |
Engine model: | Lycoming TIO-540-2AC |
Fatalities: | Fatalities: 0 / Occupants: 2 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Jackson, WY -
United States of America
|
Phase: | Landing |
Nature: | Unknown |
Departure airport: | Salt Lake City, UT (KSLC) |
Destination airport: | (KJAC) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:During a normal landing, the aircraft's nose gear collapsed. The pilots stated that three green indicator lights were observed during the final landing checklist. In postaccident troubleshooting, an instrument panel mounting screw which was too long was discovered. This screw was obstructing the movement of the landing gear selector handle to a full down position, allowing it to return prematurely to neutral (which removes hydraulic pressure from the gear system.) The nose gear was thus not hydraulically moved over center and was unlocked, even though the nose gear indicated down and locked in this configuration. Per the aircraft service manual, the nose gear linkage incorporates a downlock spring, and both gear linkage overcenter travel and gear down limit switch position are adjustable. It was not determined whether, or when, these items were checked or adjusted before the accident. After the proper screw was installed in the instrument panel, the gear operated properly in retraction tests.
Probable Cause: An improper screw installation by an unknown individual into the instrument panel, which restricted movement of the gear handle resulting in premature disengagement of the normal landing gear extension system. A factor was one or more improperly adjusted nose gear system components, which resulted in an unlocked nose gear that falsely indicated down and locked.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | SEA96LA140 |
Status: | Investigation completed |
Duration: | 1 year 1 month |
Download report: | Final report |
|
Sources:
NTSB SEA96LA140
History of this aircraft
Other occurrences involving this aircraft Location
Revision history:
Date/time | Contributor | Updates |
13-Mar-2024 14:42 |
ASN Update Bot |
Added |
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