ASN Wikibase Occurrence # 357181
This information is added by users of ASN. Neither ASN nor the Flight Safety Foundation are responsible for the completeness or correctness of this information.
If you feel this information is incomplete or incorrect, you can
submit corrected information.
Date: | Tuesday 25 June 1996 |
Time: | 18:10 LT |
Type: | Loehle 5151 RG Mustang |
Owner/operator: | Private |
Registration: | N5151N |
MSN: | 395321019 |
Total airframe hrs: | 83 hours |
Engine model: | ROTAX 582-LC |
Fatalities: | Fatalities: 0 / Occupants: 1 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Fond Du Lac, WI -
United States of America
|
Phase: | Initial climb |
Nature: | Private |
Departure airport: | (KFLD) |
Destination airport: | (KFLD) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The pilot had been flying for about 1-1/2 hours. During the initial climb following a touch and go landing, the engine sputtered and stopped running. The pilot made an off-airport forced landing. He said he had mistakenly moved the fuel selector valve to the 'OFF' position after the engine sputtered. An on-scene investigation revealed the fuel selctor valve was located under the pilot's right leg and did not have detents for the fuel tank selector positions.
Probable Cause: the pilot's improper positioning of the fuel tank selector, which resulted in fuel starvation and loss of engine power. A factor relating to the accident was: the design/location of the fuel tank selector.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | CHI96LA215 |
Status: | Investigation completed |
Duration: | 2 months |
Download report: | Final report |
|
Sources:
NTSB CHI96LA215
Location
Revision history:
Date/time | Contributor | Updates |
13-Mar-2024 15:08 |
ASN Update Bot |
Added |
The Aviation Safety Network is an exclusive service provided by:
CONNECT WITH US:
©2024 Flight Safety Foundation