ASN Wikibase Occurrence # 357276
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Date: | Saturday 8 June 1996 |
Time: | 07:45 LT |
Type: | Piper PA-32R-301 |
Owner/operator: | Private |
Registration: | N821RR |
MSN: | 3246022 |
Total airframe hrs: | 107 hours |
Engine model: | Lycoming IO-540-K1G5 |
Fatalities: | Fatalities: 0 / Occupants: 1 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | San Juan -
Puerto Rico
|
Phase: | Landing |
Nature: | Training |
Departure airport: | (KSIG) |
Destination airport: | |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:Two days before the accident, tape had been placed over each static port in preparation for washing the airplane. The person who placed the tape and the person who washed the airplane did not remove the tape after the airplane had been washed. During the preflight inspection of the airplane, the student pilot did not observe or remove the tape covering each static port. The airplane preflight inspection checklist indicates that each static port is required to be inspected to verify each is clear. The flight departed to perform touch-and-go landings and during the downwind leg, the airspeed indicator indicated 0. The pilot stated he lowered the landing gear via the normal method but the gear indicator lights circuit breaker popped several times while in the pattern. Witnesses reported hearing the airplane flying in the traffic pattern at near full power. The pilot flew over the runway and remained in the pattern. While on final approach during the second pattern, all gear indicator lights indicated that the gear was down and locked. The airplane landed hard causing all three gears to collapse and the nose baggage door to open. Flight tests confirm that the airspeed indicator would indicate during the takeoff roll until the flight was about 400 feet above ground level at which time the airspeed indicator would indicate 0. The pilot had a total of 3.6 hours total solo time in the accident airplane and no more than 15 solo landings. He did not activate the equipped alternate static source.
Probable Cause: Failure of the student pilot to maintain the proper descent rate resulting in a hard landing. Contributing to the accident was: the failure of other maintenance personnel to remove tape that was placed by company personnel over each static port before washing the airplane, inadequate preflight of the airplane by the student pilot, his failure to activate the alternate static source, and his lack of total experience in make and model airplane.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | MIA96LA152 |
Status: | Investigation completed |
Duration: | 8 months |
Download report: | Final report |
|
Sources:
NTSB MIA96LA152
Revision history:
Date/time | Contributor | Updates |
13-Mar-2024 16:08 |
ASN Update Bot |
Added |
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