ASN Wikibase Occurrence # 357493
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Date: | Friday 26 April 1996 |
Time: | 16:35 LT |
Type: | Cessna 210M |
Owner/operator: | Private |
Registration: | N722PD |
MSN: | 21061664 |
Total airframe hrs: | 2940 hours |
Engine model: | Continental IO-520-L |
Fatalities: | Fatalities: 0 / Occupants: 1 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Meridian, MS -
United States of America
|
Phase: | En route |
Nature: | Private |
Departure airport: | (KMEI) |
Destination airport: | Olive Branch, MS (OLV |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The pilot, who had previously flown the airplane, reported that he had an oil leak and landed at Meridian. He found oil on the engine cowling behind the propeller, and thought the propeller oil seal was leaking. He added 2 quarts of oil, and took off on another flight. During climb-out, the oil pressure dropped below the red line, and the pilot returned to Meridian and landed after about a 10 to 15 minute flight. He did not inform the owners or mechanics that he had operated the engine with low oil pressure, while returning to the airport. Mechanics found a cracked oil cooler. They replaced the oil cooler and added about 8 quarts of oil to fill the engine to 9 quarts. Another pilot went to Meridian to ferry the plane back to the home base. He reported that during the climb after departure, the engine began to vibrate and loose power. He turned back, but did not have enough power to reach the airport. The engine seized, and during an emergency landing, the aircraft encountered a ditch and nosed over. Postcrash examination of the engine showed the #5 connecting rod had failed due to damage from oil starvation. The other connecting rod bearings also showed indications of oil starvation, and debris was found in the oil pump and filter.
Probable Cause: previous engine damage; failure of the pilot of the previous flight to report to the operator and/or mechanics that the engine had been operated with low (or no) oil pressure; inadequate maintenance/inspection after most of the oil had leaked from the engine oil system during the previous flight; oil starvation; and subsequent failure of the #5 connecting rod. Factors relating to the accident were: the previous oil filter leak and loss of oil pressure.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | MIA96LA131 |
Status: | Investigation completed |
Duration: | 5 months |
Download report: | Final report |
|
Sources:
NTSB MIA96LA131
Location
Revision history:
Date/time | Contributor | Updates |
13-Mar-2024 18:28 |
ASN Update Bot |
Added |
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