Accident Hughes 369D N519BH,
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ASN Wikibase Occurrence # 357546
 
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Date:Sunday 14 April 1996
Time:11:55 LT
Type:Silhouette image of generic H500 model; specific model in this crash may look slightly different    
Hughes 369D
Owner/operator:William Barron Hilton
Registration: N519BH
MSN: 854D
Total airframe hrs:1793 hours
Engine model:Allison 250-C20B
Fatalities:Fatalities: 0 / Occupants: 3
Aircraft damage: Substantial
Category:Accident
Location:Yerington, NV -   United States of America
Phase: En route
Nature:Private
Departure airport:, NV
Destination airport:
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
The pilot experienced a total loss of engine power while cruising between 200 and 300 feet above ground level and at an airspeed of 100 knots. The pilot reported that the engine noise resembled the same whining as if it were in a shut down mode. The pilot entered an autorotation and landed in an open field approximately 0.5 miles from his airstrip. The accident site examination revealed that the helicopter had touched down with forward speed and made depressions in the soft ground over a distance of 25 to 30 feet. The helicopter rolled onto its side and a main rotor blade severed the tail boom. Tail rotor blade and drive shaft components separated from the helicopter and were found 200 feet from the main wreckage. The last annual inspection was performed 6 months prior to the accident flight and the aircraft had flown 16.9 hours. Also, the last compressor wash was performed about 2 months prior to the flight and had flown 8 hours since then. The postaccident engine examination revealed accumulated nozzle port debris and dirty compressor blades and vanes. The engine flamed out during its first test run and, during subsequent tests, it produced power 7.8 percent below specifications.

Probable Cause: the partial loss of engine power and the pilot's misjudged flare during an autorotation landing in soft dirt with excessive forward speed. The power loss resulted from flight operations in an environment which debris contaminated the engine's nozzle port and compressor assembly.

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: LAX96LA168
Status: Investigation completed
Duration: 8 months
Download report: Final report

Sources:

NTSB LAX96LA168

Location

Revision history:

Date/timeContributorUpdates
13-Mar-2024 19:07 ASN Update Bot Added

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