Serious incident Avro RJ70 N832BE,
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ASN Wikibase Occurrence # 357751
 
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Date:Tuesday 20 February 1996
Time:22:58 LT
Type:Silhouette image of generic RJ70 model; specific model in this crash may look slightly different    
Avro RJ70
Owner/operator:Business Express Airlines
Registration: N832BE
MSN: E1223
Total airframe hrs:3925 hours
Engine model:Lycoming LF-507-1F
Fatalities:Fatalities: 0 / Occupants: 28
Aircraft damage: None
Category:Serious incident
Location:Rifle, CO -   United States of America
Phase: Landing
Nature:Unknown
Departure airport:Minneapolis, MN (MSP
Destination airport:(KRIL)
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
The first officer, who flew the LOC/DME-A approach to runway 26 at a Vref speed of 115 5 knots, said the airplane touched down 2500 feet past the threshold and went off the end of the 7000 foot runway, coming to a halt 300 feet beyond. The airport manager said, and FDR and GPS confirmed, the airplane touched down 4600 feet beyond the runway threshold at 138 knots ground speed and 119 knots indicated airspeed, and traveled 3400 feet before coming to a halt. Prior to landing, the crew did not request, nor did the airport or company dispatch give, runway condition, braking action, or precipitation reports. The captain said he found one inch of slush on the runway. The Airplane Flight Manual states landings 'on a slippery surface having a braking coefficient of friction of 0.05...are not permitted on a downhill runway unless the downhill slope is less than 0.5% and there is no tailwind component.' Runway 26 has a 1.2% downhill gradient and FDR data indicates the wind was 098 at 6 knots.

Probable Cause: The copilot's failure to compensate for wind conditions, resulting in excessive airspeed, and his failure to attain the proper runway touch down point. Factors were inadequate dispatch procedures and the captain's improper inflight planning/decision in that runway conditions were not requested or obtained; a tail wind, a wet downhill runway, hydroplaning conditions, and the captain's failure to adequately supervise the copilot.

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: FTW96IA124
Status: Investigation completed
Duration: 4 months
Download report: Final report

Sources:

NTSB FTW96IA124

Location

Revision history:

Date/timeContributorUpdates
14-Mar-2024 06:13 ASN Update Bot Added

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