Serious incident Boeing 737-130 N33202,
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ASN Wikibase Occurrence # 357753
 
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Date:Tuesday 20 February 1996
Time:16:12 LT
Type:Silhouette image of generic B731 model; specific model in this crash may look slightly different    
Boeing 737-130
Owner/operator:Continental Airlines
Registration: N33202
MSN: 19019/10
Total airframe hrs:1118 hours
Engine model:P&W JT8D-7
Fatalities:Fatalities: 0 / Occupants: 79
Aircraft damage: Minor
Category:Serious incident
Location:Washington, DC -   United States of America
Phase: Landing
Nature:Unknown
Departure airport:Greensboro, NC (GSO
Destination airport:(KDCA)
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
The pilots reported that as they neared the destination airport, ATC requested that they keep their airspeed up during the approach. The pilots obtained the current ATIS information, which noted an 'overriding tailwind component' on final approach for runway 36. The surface winds were reported to be from 040 degrees at 7 knots. The captain indicated that he began to slow the airplane for landing during the descent, about 11 miles south of the airport. ATC personnel in the tower indicated that the airplane was fast on the approach, and it touched down slightly farther down the runway than other airplanes that landed that day. They also indicated that the thrust reversers deployed farther down the runway than usual. FDR data indicated that the airplane touched down at about 180 knots indicated airspeed. The FDR data also showed that during the previous landing (made by another aircrew), the airplane touched down at about 140 knots. Subsequently, the airplane ran off the departure end of the runway and stopped about 250 feet onto the overrun area where it encountered mud. Postaccident examination revealed that the two inboard main landing gear tires had blown out during the landing. During a test of the anti-skid system, the channel for the inboard brakes did not function properly.

Probable Cause: excessive airspeed was maintained by the captain during the approach/landing phase of the flight, which resulted in an overrun and an encounter with soft/wet terrain. Factors relating to the incident were: the pilot's failure to attain the proper touchdown point, the wet runway condition, and partial failure of the anti-skid brake system.

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: IAD96IA044
Status: Investigation completed
Duration: 10 months
Download report: Final report

Sources:

NTSB IAD96IA044

Location

Revision history:

Date/timeContributorUpdates
14-Mar-2024 06:13 ASN Update Bot Added

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