ASN Wikibase Occurrence # 357890
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Date: | Thursday 28 December 1995 |
Time: | 12:00 LT |
Type: | Bellanca 7GCBC |
Owner/operator: | Leroy Nielson |
Registration: | N88384 |
MSN: | 774-75 |
Year of manufacture: | 1974 |
Total airframe hrs: | 1084 hours |
Engine model: | LYCOMING O-320-A2B |
Fatalities: | Fatalities: 0 / Occupants: 2 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Munich, ND -
United States of America
|
Phase: | Approach |
Nature: | Unknown |
Departure airport: | Devils Lake, ND (KDVL) |
Destination airport: | |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:While making a precautionary landing the pilot applied carburetor heat during the downwind leg of his approach to a road. It was removed a short time later. While on final approach the pilot said the airplane began descending too rapidly. He said he applied power and the engine did not respond. The pilot said the airplane drifted to the right as it neared the road. He said he applied left aileron and it continued to drift to the right. The pilot said he could not recall if he had applied right rudder when he applied left aileron. The pilot said the ailerons didn't respond because the airplane was too slow. The airplane landed in snow next to the road and nosed over. The on-scene investigation found no mechanical anomalies that would prevent normal flight. According to pilot/operator handbook for the Bellanca 7GCBC, the pilot is directed to use carburetor heat only when 'atmospheric conditions indicate that icing is probable....' The temperature and dew point were 17 and 12 degress F. respectively. The FAA's carburetor icing chart shows carburetor icing was probable.
Probable Cause: the pilot allowed his airspeed to get too low and encountered a stall/mush condition. Factors associated with the accident were the pilot not being able to maintain directional control due to misuse of the controls for wind drift correction and improper use of the carburetor heat.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | CHI96LA064 |
Status: | Investigation completed |
Duration: | 3 months |
Download report: | Final report |
|
Sources:
NTSB CHI96LA064
History of this aircraft
Other occurrences involving this aircraft Location
Revision history:
Date/time | Contributor | Updates |
14-Mar-2024 07:43 |
ASN Update Bot |
Added |
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