ASN Wikibase Occurrence # 357900
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Date: | Tuesday 26 December 1995 |
Time: | 11:00 LT |
Type: | Cessna 182Q |
Owner/operator: | Private |
Registration: | N97196 |
MSN: | 18267011 |
Year of manufacture: | 1979 |
Total airframe hrs: | 1400 hours |
Engine model: | Continental O-470-U |
Fatalities: | Fatalities: 0 / Occupants: 3 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Fallbrook, CA -
United States of America
|
Phase: | Landing |
Nature: | Private |
Departure airport: | Long Beach, CA (KLGB) |
Destination airport: | (L18) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:After arriving over the airport, the pilot was unsuccessful in obtaining an airport advisory by using the common traffic advisory frequency (CTAF) from a flight information publication that was in his possession. (After the accident, he noticed the publication was out-of-date and did not have the correct CTAF published.) The pilot said he could find no means for determining the wind direction, and he elected to land on runway 18. During the landing roll, he was unable to stop the aircraft on the remaining runway, and it overran the departure end, encountered a rough surface, and nosed over. The pilot said that after the accident, he realized he had unknowingly landed downwind with a 15-knot tail wind. Ground witnesses reported that the aircraft was very fast and had touched down about 1,000 feet down the 2,160-foot-long runway. The witnesses also stated that the winds had been steady from the north at 10 to 15 knots all morning.
Probable Cause: the pilot's inadequate preflight planning/preparation (failure to ensuring the flight information publication was current); his selection of the wrong runway for landing; his failure to achieve the proper touchdown point during the landing; and his failure to go around, while there was still sufficient airspeed and runway available. The tailwind was a related factor.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | LAX96LA079 |
Status: | Investigation completed |
Duration: | 5 months |
Download report: | Final report |
|
Sources:
NTSB LAX96LA079
Location
Revision history:
Date/time | Contributor | Updates |
14-Mar-2024 07:49 |
ASN Update Bot |
Added |
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