ASN Wikibase Occurrence # 357919
This information is added by users of ASN. Neither ASN nor the Flight Safety Foundation are responsible for the completeness or correctness of this information.
If you feel this information is incomplete or incorrect, you can
submit corrected information.
Date: | Saturday 16 December 1995 |
Time: | 16:20 LT |
Type: | Bellanca 7ECA |
Owner/operator: | Private |
Registration: | N990WY |
MSN: | 1168-76 |
Year of manufacture: | 1976 |
Total airframe hrs: | 280 hours |
Engine model: | LYCOMING O-235-C1 |
Fatalities: | Fatalities: 0 / Occupants: 1 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Mason, MI -
United States of America
|
Phase: | Take off |
Nature: | Private |
Departure airport: | |
Destination airport: | |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:The pilot was making a touch-and-go from his home strip. He planned his pattern so as to touch down fast to practice a two-wheel touch-and-go. The airplane touched down halfway down the strip. When the pilot applied power for takeoff, the engine did not respond. The pilot described the engine's sound as being 'like someone putting a hand over the carburetor. It (the engine) was going, but not picking up any rpm.' The pilot advanced the throttle, retarded it and then advanced it again. Because the airplane was now two-thirds of the way down the runway, the pilot continued the takeoff. The pilot's private strip has a powerline which crosses over the strip 175 feet prior to the end. As the airplane went under the powerline, the engine responded with full power, and the airplane's left wing struck a utility pole which supports the powerline along the side of the strip. The airplane struck two trees and a wood fence before it nosed over in a ditch along the side of a road. Examination of the wreckage disclosed flight control continuity and no mechanical anomalies in the engine and engine controls.
Probable Cause: the improper application of the throttle by the pilot resulting in a delayed engine response, and the improper decision by the pilot to make a long fast touchdown requiring the need to take off under powerlines.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | CHI96LA055 |
Status: | Investigation completed |
Duration: | 3 months |
Download report: | Final report |
|
Sources:
NTSB CHI96LA055
History of this aircraft
Other occurrences involving this aircraft
3 October 2013 |
N990WY |
AeroDynamic Aviation |
0 |
Capitol Expressway, San Jose, CA |
|
non |
Location
Revision history:
Date/time | Contributor | Updates |
14-Mar-2024 08:02 |
ASN Update Bot |
Added |
The Aviation Safety Network is an exclusive service provided by:
CONNECT WITH US:
©2024 Flight Safety Foundation