Accident Piper PA-28R-180 N3250R,
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ASN Wikibase Occurrence # 358157
 
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Date:Friday 13 October 1995
Time:15:37 LT
Type:Silhouette image of generic P28R model; specific model in this crash may look slightly different    
Piper PA-28R-180
Owner/operator:Southwest Florida Air
Registration: N3250R
MSN: 28R-31251
Total airframe hrs:6234 hours
Engine model:Lycoming IO-360-B1E
Fatalities:Fatalities: 0 / Occupants: 4
Aircraft damage: Substantial
Category:Accident
Location:Covington, GA -   United States of America
Phase: Landing
Nature:Private
Departure airport:Clearwater, FL (CLW
Destination airport:Atlanta, GA (KPDK)
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
The flight departed with less than full fuel due to weight and balance considerations. En route, the pilot recognized a fuel shortage condition existed while the flight was near an airport with an ILS approach. The flight continued, and the pilot advised that the frequency congestion increased and ATC control was transferred to several sectors. The pilot then declared minimum fuel to the controller after he was advised that the flight was 50 miles from the planned destination. The controller vectored the flight to a nearby airport with an instrument approach, and while descending toward that airport, the engine sputtered momentarily then regained power when the fuel selector was positioned to the opposite tank. The pilot then declared an emergency and the flight was vectored direct toward the airport. After descending below the base of the clouds, the engine again sputtered. The pilot landed the airplane in a field with uneven terrain. It collided with an elevated gravel road, separating the nose gear, and became airborne. The airplane touched down again and the left main landing gear collapsed. Postcrash examination revealed that the fuel selector was positioned to the right fuel tank which was found to contain 3.5 gallons of fuel. The left wing fuel tank was empty.

Probable Cause: the pilot's failure to divert to an alternate airport after recognizing a low fuel state existed and his delay to declare an emergency with ATC. Contributing to the accident was the unsuitable terrain encountered during the forced landing.

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: MIA96LA008
Status: Investigation completed
Duration: 1 year
Download report: Final report

Sources:

NTSB MIA96LA008

Revision history:

Date/timeContributorUpdates
14-Mar-2024 10:30 ASN Update Bot Added

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