ASN Wikibase Occurrence # 358243
This information is added by users of ASN. Neither ASN nor the Flight Safety Foundation are responsible for the completeness or correctness of this information.
If you feel this information is incomplete or incorrect, you can
submit corrected information.
Date: | Saturday 23 September 1995 |
Time: | 10:30 LT |
Type: | Piper PA-32-260 |
Owner/operator: | Pompano Senior Squadron Flying |
Registration: | N40971 |
MSN: | 32-7400026 |
Total airframe hrs: | 6539 hours |
Engine model: | LYCOMING O-540-E4B5 |
Fatalities: | Fatalities: 0 / Occupants: 2 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | St. Augustine, FL -
United States of America
|
Phase: | Approach |
Nature: | Private |
Departure airport: | Pompano, FL (KPMP) |
Destination airport: | (KSGJ) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:THE FLIGHT DEPARTED WITH FULL FUEL TANKS AND THE PILOT STATED THAT ABOUT 1 HOUR AFTER TAKEOFF HE REPOSITIONED THE FUEL SELECTOR FROM THE RIGHT TANK TO THE LEFT TANK. THE FLIGHT CONTINUED, ENTERED THE TRAFFIC PATTERN TO LAND, AND THE PILOT EXTENDED THE DOWNWIND LEG DUE TO TRAFFIC. THE FLIGHT THEN TURNED LEFT BASE AND THE ENGINE FAILED TO RESPOND TO THROTTLE INPUT. THE AIRPLANE COLLIDED WITH TREES DURING THE FORCED LANDING. THE AIRPLANE WAS RECOVERED AND BOTH FUEL TANKS WERE FOUND TO BE RUPTURED. THE FUEL SELECTOR WAS FOUND POSITIONED TO THE RIGHT FUEL TANK. THE FUEL LINE TO THE INLET OF THE CARBURETOR AND CARBURETOR BOWL WERE DRAINED AND CONTAINED ABOUT 1-2 OUNCES OF FUEL EACH. NO FUEL CONTAMINATION NOR OBSTRUCTIONS OF THE FUEL SUPPLY SYSTEM WERE NOTED. AN UNDAMAGED PROPELLER WAS INSTALLED AS WELL AS AN AUXILIARY FUEL TANK AND THE ENGINE WAS STARTED AND FOUND TO OPERATE NORMALLY.
Probable Cause: FUEL STARVATION FOR UNDETERMINED REASONS RESULTING IN THE TOTAL LOSS OF ENGINE POWER. CONTRIBUTING TO THE ACCIDENT WAS UNSUITABLE TERRAIN ENCOUNTERED DURING THE FORCED LANDING.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | MIA95LA231 |
Status: | Investigation completed |
Duration: | 2 months |
Download report: | Final report |
|
Sources:
NTSB MIA95LA231
Location
Revision history:
Date/time | Contributor | Updates |
14-Mar-2024 11:22 |
ASN Update Bot |
Added |
The Aviation Safety Network is an exclusive service provided by:
CONNECT WITH US:
©2024 Flight Safety Foundation