Accident Quad City Challenger II N4281D,
ASN logo
ASN Wikibase Occurrence # 358315
 
This information is added by users of ASN. Neither ASN nor the Flight Safety Foundation are responsible for the completeness or correctness of this information. If you feel this information is incomplete or incorrect, you can submit corrected information.

Date:Sunday 3 September 1995
Time:18:53 LT
Type:Silhouette image of generic quad model; specific model in this crash may look slightly different    
Quad City Challenger II
Owner/operator:Private
Registration: N4281D
MSN: CH1290CW599
Engine model:ROTAX 503
Fatalities:Fatalities: 0 / Occupants: 1
Aircraft damage: Substantial
Category:Accident
Location:Cedar Springs, MI -   United States of America
Phase: Initial climb
Nature:Private
Departure airport:, MI (KRLA)
Destination airport:
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
WITNESSES STATED THE HOMEBUILT AIRPLANE'S ENGINE BEGAN SPUTTERING DURING ITS INITIAL CLIMB AFTER TAKEOFF AND THE AIRPLANE CIRCLED BACK TOWARD THE AIRPORT FOR A LANDING. DURING ITS APPROACH THE AIRPLANE'S TAIL WHEEL STRUCK A POWER LINE AND THE AIRPLANE PITCHED DOWN AND COLLIDED WITH THE GROUND. THE ON-SCENE INVESTIGATION REVEALED CONTROL CABLE CONTINUITY WITH THEIR RESPECTIVE CONTROL SURFACES, AND FOUR FOULED SPARK PLUGS, TWO THAT HAD NO VISIBLE ELECTRODE GAP. THE PILOT SAID THE PLUGS DIDN'T HAVE TO BE CLEANED OR CHANGED UNTIL THEY OPERATED FOR 50 HOURS. THE PILOT SAID THE PLUGS HAD BEEN USED ABOUT 50 HOURS. AN ENGINE MANUFACTURER'S REPRESENTATIVE SAID THE PLUGS NEED TO BE CHANGED AFTER 25 HOURS OF ENGINE RUNNING TIME. THE REPRESENTATIVE SAID THE ENGINE MUST BE DECARBONIZED AFTER 50 HOURS OF OPERATION. THE PROCEDURE IS TO INSPECT THE ENGINE AFTER DISMANTLING THE CYLINDERS, HEADS, AND PISTONS. THE OWNER/PILOT SAID HE CHECKED FOR CARBONIZATION BY LOOKING IN THE EXHAUST PORT. THE REPRESENTATIVE SAID THIS IS NOT THE CORRECT PROCEDURE.

Probable Cause: inadequate engine maintenance by the owner/pilot-mechanic. Factors associated with the accident were fouled spark plugs and the pilot not being able to maintain proper altitude/clearance between his airplane and the electrical power lines during his landing approach.

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: CHI95LA293
Status: Investigation completed
Duration: 7 months
Download report: Final report

Sources:

NTSB CHI95LA293

Location

Revision history:

Date/timeContributorUpdates
14-Mar-2024 12:12 ASN Update Bot Added

Corrections or additions? ... Edit this accident description

The Aviation Safety Network is an exclusive service provided by:
Quick Links:

CONNECT WITH US: FSF on social media FSF Facebook FSF Twitter FSF Youtube FSF LinkedIn FSF Instagram

©2024 Flight Safety Foundation

1920 Ballenger Av, 4th Fl.
Alexandria, Virginia 22314
www.FlightSafety.org