Accident Piper PA-32R N39620,
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ASN Wikibase Occurrence # 358815
 
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Date:Friday 23 June 1995
Time:15:10 LT
Type:Silhouette image of generic P32R model; specific model in this crash may look slightly different    
Piper PA-32R
Owner/operator:Private
Registration: N39620
MSN: 32R-7887123
Total airframe hrs:1766 hours
Engine model:LYCOMING TIO-540-S1AD
Fatalities:Fatalities: 0 / Occupants: 2
Aircraft damage: Substantial
Category:Accident
Location:Columbia, MO -   United States of America
Phase: En route
Nature:Private
Departure airport:Iowa City, IA (KIOW)
Destination airport:Point Lookout, MO
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
THE PILOT REPORTED THAT HE HEARD A MUFFLED EXPLOSION FROM THE ENGINE COMPARTMENT. THE ENGINE QUIT AND FLAMES STARTED COMING OUT OF THE ENGINE COWLING. THE CABIN BEGAN FILLING WITH SMOKE, AND OIL BEGAN SPEWING ONTO THE WINDSCREEN. THE PILOT SUCCESSFULLY EXECUTED PROCEDURES FOR IN-FLIGHT FIRE AND SMOKE IN THE COCKPIT. HE THEN MADE AN EMERGENCY LANDING IN A FIELD. HOWEVER, BEFORE LANDING, THE PILOT DELAYED GEAR EXTENSION, SO THAT HE COULD REMAIN CLEAR OF OBSTRUCTIONS AND REACH A SUITABLE LANDING AREA. THE GEAR DID NOT HAVE ENOUGH TIME TO BE FULLY EXTENDED, AND IT COLLAPSED ON TOUCHDOWN. AN EXAMINATION OF THE AIRPLANE REVEALED THAT THE DUAL MAGNETO HAD SEPARATED FROM THE ENGINE. THE BOTTOM MAGNETO HOLD DOWN CLIP WAS FOUND IN THE COWLING, BUT NEITHER THE LOCKWASHER OR NUT WERE RECOVERED. AN EXAMINATION OF THE BOTTOM SURFACE OF THE MAGNETO HOUSING REVEALED TWO LONGITUDINAL MARKINGS (CHIPPED PAINT). THE BOTTOM CLIP HAD A SPACING WHICH MATCHED THE CHIPPED PAINT ON THE MAGNETO HOUSING, AS IF THE CLIP HAD MOVED LONGITUDINALLY RELATIVE TO THE HOUSING. AN EXAMINATION OF THE TOP MAGNETO HOUSING FLANGE, WHICH HAD SEPARATED FROM THE MAGNETO, REVEALED FRACTURE SURFACE MARKINGS INDICATIVE OF FATIGUE CRACKING BEFORE THE ONSET OF OVERSTRESS SEPARATION.

Probable Cause: A LOOSE (OR MISSING) NUT AND CLIP FOR THE BOTTOM MAGNETO STUD, DUE TO INADEQUATE MAINTENANCE, AND FATIGUE FAILURE OF THE MAGNETO HOUSING FLANGE, WHICH RESTULTED IN AN OIL LEAK, ENGINE COMPARTMENT FIRE, AND A FORCED LANDING. A FACTOR RELATING TO THE ACCIDENT WAS: THE NECESSITY FOR THE PILOT TO DELAY EXTENDING THE LANDING GEAR, SO THAT THE AIRPLANE WOULD CLEAR OBSTRUCTIONS AND REACH A FAVORABLE LANDING AREA.

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: CHI95LA196
Status: Investigation completed
Duration: 8 months
Download report: Final report

Sources:

NTSB CHI95LA196

Revision history:

Date/timeContributorUpdates
14-Mar-2024 18:28 ASN Update Bot Added

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