Accident Hughes 500D N549SW,
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ASN Wikibase Occurrence # 358868
 
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Date:Monday 12 June 1995
Time:05:15 LT
Type:Silhouette image of generic H500 model; specific model in this crash may look slightly different    
Hughes 500D
Owner/operator:Silver Bay Logging Inc.
Registration: N549SW
MSN: 800754D
Total airframe hrs:4278 hours
Engine model:Allison250-C20B
Fatalities:Fatalities: 0 / Occupants: 4
Aircraft damage: Substantial
Category:Accident
Location:Ketchikan, AK -   United States of America
Phase: En route
Nature:Unknown
Departure airport:Fire Cove, AK
Destination airport:
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
THE HELICOPTER PILOT WAS IN CRUISE FLIGHT ABOUT 250 FEET ABOVE THE GROUND, TRANSPORTING LOGGING PERSONNEL TO A REMOTE AREA. THE ENGINE SUDDENLY LOST POWER, AND THE PILOT BEGAN AN AUTOROTATION TO A GRAVEL PIT. DURING TOUCHDOWN, THE TAILBOOM WAS SEVERED, AND THE HELICOPTER ROLLED ONTO ITS RIGHT SIDE. DURING RECOVERY OF THE HELICOPTER, THE LIFTING CABLE BROKE, AND THE HELICOPTER DESCENDED TO THE GROUND FROM ABOUT 400 FEET. POSTACCIDENT EXAMINATION OF THE ENGINE FUEL CONTROL AND POWER TURBINE GOVERNOR DID NOT REVEAL ANY MALFUNCTION. EXAMINATION OF THE PNEUMATIC PC TUBE (AIR LINE) FROM THE PC FILTER TO THE GOVERNOR REVEALED AN AIR LEAK AT THE 'B' NUT ATTACHMENT TO THE GOVERNOR 'T' FITTING. LABORATORY TESTING REVEALED THAT A TORQUE OF 300 INCH POUNDS WOULD HAVE BEEN REQUIRED TO STOP THE AIR LEAK. THE MANUFACTURER'S SPECIFIED TORQUE VALUE WAS 100 INCH POUNDS. RECORDS SHOWED THAT ON 6/7/95, MAINTENANCE HAD BEEN PERFORMED TO REPLACE THE GOVERNOR AND TO CLEAN AND REINSTALL THE P2 AIR LINE; AND ON 6/11/95 (DAY BEFORE THE ACCIDENT), THE ENGINE SPEED HAD BEEN ADJUSTED. THE MAINTENANCE MANUAL FOR THE ENGINE WARNED THAT AIR LEAKS IN THE PNEUMATIC SENSING SYSTEM COULD RESULT IN FLAME-OUT, POWER LOSS, OR OVERSPEED.

Probable Cause: AN AIR LEAK AT A 'B' NUT FITTING ON A PNEUMATIC PC TUBE TO THE POWER TURBINE GOVERNOR. COMPANY MAINTENANCE PERSONNEL DID NOT DETECT A LEAK AFTER PERFORMING MAINTENANCE ON THE GOVERNER AND P2 AIR LINE.

Accident investigation:
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Investigating agency: NTSB
Report number: ANC95LA075
Status: Investigation completed
Duration: 8 months
Download report: Final report

Sources:

NTSB ANC95LA075

Location

Revision history:

Date/timeContributorUpdates
14-Mar-2024 19:07 ASN Update Bot Added

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