ASN Wikibase Occurrence # 359267
This information is added by users of ASN. Neither ASN nor the Flight Safety Foundation are responsible for the completeness or correctness of this information.
If you feel this information is incomplete or incorrect, you can
submit corrected information.
Date: | Wednesday 8 March 1995 |
Time: | 19:00 LT |
Type: | Cessna 337C |
Owner/operator: | B & J Worrell Flying Service |
Registration: | N2621S |
MSN: | 337-0921 |
Year of manufacture: | 1968 |
Total airframe hrs: | 2421 hours |
Engine model: | CONTINENTAL IO-360-C |
Fatalities: | Fatalities: 0 / Occupants: 2 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Porter, TX -
United States of America
|
Phase: | Landing |
Nature: | Private |
Departure airport: | (9XS2) |
Destination airport: | |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:THE PILOT INADVERTENTLY LANDED THE AIRPLANE GEAR-UP. THE PILOT REPORTED THAT HE WAS DISTRACTED BY A FLAPPING NOISE AND FORGOT TO VISUALLY CHECK THE POSITION OF THE LANDING GEAR. HE TOLD HIS MECHANIC THAT THERE WAS NOTHING WRONG WITH THE LANDING GEAR SYSTEM. A STRUCTURAL BOX BEAM WAS DAMAGED DURING GROUND SLIDE.
Probable Cause: THE PILOT'S FAILURE TO EXTEND THE LANDING GEAR. FACTORS WERE HIS FAILURE TO USE A CHECKLIST AND HIS DIVERTED ATTENTION.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | FTW95LA133 |
Status: | Investigation completed |
Duration: | 5 months |
Download report: | Final report |
|
Sources:
NTSB FTW95LA133
Location
Revision history:
Date/time | Contributor | Updates |
15-Mar-2024 08:43 |
ASN Update Bot |
Added |
The Aviation Safety Network is an exclusive service provided by:
CONNECT WITH US:
©2024 Flight Safety Foundation