ASN Wikibase Occurrence # 359406
This information is added by users of ASN. Neither ASN nor the Flight Safety Foundation are responsible for the completeness or correctness of this information.
If you feel this information is incomplete or incorrect, you can
submit corrected information.
Date: | Saturday 21 January 1995 |
Time: | 11:30 LT |
Type: | Piper PA-31-350 |
Owner/operator: | Airpac Airlines Inc. |
Registration: | N36PB |
MSN: | 31-7405128 |
Year of manufacture: | 1973 |
Total airframe hrs: | 11922 hours |
Engine model: | LYCOMING TIO-540-J2BD |
Fatalities: | Fatalities: 0 / Occupants: 1 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | La Grande, OR -
United States of America
|
Phase: | Approach |
Nature: | Ferry/positioning |
Departure airport: | Pendleton, OR (KPDT) |
Destination airport: | (KLGD) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:THE PILOT REPORTED THAT WHILE FLYING THE NDB APPROACH IN IMC, HE NOTED THAT THE IDENTIFYING SIGNAL WAS WEAK AND THE ADF NEEDLE WANDERED. HE CONTINUED THE APPROACH, BUT DID NOT DESCEND BELOW THE MINIMUM DESCENT ALTITUDE OF 4000' MSL. WHEN HE FELT THAT HE WAS OVER THE RUNWAY, HE LOOKED DOWN AND SAW TREES THROUGH THE FOG. IMMEDIATELY THEREAFTER, HE FELT THE AIRPLANE HIT SOMETHING. THE PILOT PERFORMED A MISSED APPROACH AND DIVERTED TO ANOTHER AIRPORT, WHERE HE LANDED WITHOUT FURTHER INCIDENT. AN EXAM OF THE AIRPLANE REVEALED EVIDENCE THAT IT HAD COLLIDED WITH A TREE. AN INVESTIGATION REVEALED THAT THE NDB WAS OUT OF SERVICE, AND NO NOTAM HAD BEEN ISSUED. THE PARTY RESPONSIBLE FOR REPORTING THE SERVICEABILITY OF THE NDB REPORTED TO THE FSS THAT THE 'BEACON' WAS OUT OF SERVICE. THE FSS INTERPRETED 'BEACON' AS THE 'ROTATING BEACON' ON THE AIRPORT. THE AIRPORT WAS LOCATED IN A VALLEY AT AN ELEVATION OF 2714'. THE NDB APPROACH TO THE AIRPORT WAS FROM THE NORTH. HIGH TERRAIN TO ABOUT 6000' MSL WAS LOCATED TO THE EAST AND WEST OF THE AIRPORT. THE INVESTIGATION DID NOT REVEAL THE EXACT LOCATION OF IMPACT WITH TREE(S).
Probable Cause: FAILURE OF THE PILOT TO MAINTAIN PROPER ALTITUDE/CLEARANCE FROM HIGHER TERRAIN THAT WAS LOCATED NEAR THE AIRPORT. FACTORS RELATED TO THE ACCIDENT WERE: LOW CEILING, FOG, FALSE/INCORRECT INDICATION OF THE NDB, FAILURE OF OTHER PERSONNEL TO PROPERLY ISSUE A NOTAM CONCERNING THE NDB, AND FAILURE OF THE PILOT TO PROPERLY IDENTIFY THE NAVAID SIGNAL.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | SEA95LA039 |
Status: | Investigation completed |
Duration: | 6 months |
Download report: | Final report |
|
Sources:
NTSB SEA95LA039
Location
Revision history:
Date/time | Contributor | Updates |
15-Mar-2024 10:12 |
ASN Update Bot |
Added |
The Aviation Safety Network is an exclusive service provided by:
CONNECT WITH US:
©2024 Flight Safety Foundation