ASN Wikibase Occurrence # 359411
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Date: | Thursday 19 January 1995 |
Time: | 10:40 LT |
Type: | Boeing 737-247 |
Owner/operator: | Air South Airlines |
Registration: | N4515W |
MSN: | 19612/93 |
Year of manufacture: | 1968 |
Total airframe hrs: | 37421 hours |
Engine model: | P&W JT8D-9A |
Fatalities: | Fatalities: 0 / Occupants: 28 |
Aircraft damage: | Minor |
Category: | Serious incident |
Location: | Atlanta, GA -
United States of America
|
Phase: | Landing |
Nature: | Unknown |
Departure airport: | Columbia, SC (KCAE) |
Destination airport: | (KATL) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:THE FLIGHT CREW REPORTED THAT THE FLIGHT PROCEEDED NORMALLY UNTIL THE LANDING ROLL. THE FIRST OFFICER FELT THE ANTISKID RELEASING, AND THE CAPTAIN TOOK OVER THE CONTROLS. BRAKING ACTION WAS INITIALLY FELT, THEN ALL BRAKING ACTION WAS LOST. THE AIRCRAFT DEPARTED THE END OF THE RUNWAY, AND CAME TO A STOP ABOUT 200 FEET PAST THE DEPARTURE END, IN THE GRASS. THE LEFT OUTBOARD MAIN TIRE WAS BLOWN. EXAMINATION OF THE AIRCRAFT REVEALED THAT THE LEFT, INBOARD ANTISKID VALVE BRAKE AND RETURN LINES WERE CROSSED. THE LEFT, INBOARD SKID DETECT CIRCUIT WAS FOUND INOPERATIVE. ALSO, THE WIRING TO THE LEFT, INBOARD AND LEFT, OUTBOARD WHEEL SPEED TRANSDUCERS WERE CROSSED. THERE WAS ALSO EVIDENCE THAT THE AIRCRAFT HAD HYDROPLANED NEAR THE DEPARTURE END OF THE RUNWAY. THE AIRCRAFT DISCREPANCIES WERE NOT DISCOVERED DURING ANTISKID SYSTEM TESTING PERFORMED ABOUT 2 WEEKS PRIOR TO THE ACCIDENT.
Probable Cause: THE INADEQUATE INSPECTION OF THE AIRCRAFT BY OTHER MAINTENANCE PERSONNEL, IN THAT THEY DID NOT PROPERLY DIAGNOSE DISCREPANCIES IN THE ANTISKID BRAKING SYSTEM.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | ATL95IA043 |
Status: | Investigation completed |
Duration: | 8 months |
Download report: | Final report |
|
Sources:
NTSB ATL95IA043
Revision history:
Date/time | Contributor | Updates |
15-Mar-2024 10:13 |
ASN Update Bot |
Added |
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