ASN Wikibase Occurrence # 359533
This information is added by users of ASN. Neither ASN nor the Flight Safety Foundation are responsible for the completeness or correctness of this information.
If you feel this information is incomplete or incorrect, you can
submit corrected information.
Date: | Saturday 26 November 1994 |
Time: | 13:02 LT |
Type: | Boeing 737-3T0 |
Owner/operator: | Continental Airlines |
Registration: | N14336 |
MSN: | 23574/1328 |
Total airframe hrs: | 26118 hours |
Engine model: | CFM 56 |
Fatalities: | Fatalities: 0 / Occupants: 134 |
Aircraft damage: | Minor |
Category: | Serious incident |
Location: | Houston, TX -
United States of America
|
Phase: | Standing |
Nature: | Unknown |
Departure airport: | |
Destination airport: | Chicago, IL (KORD) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:TWO MECHANICS WERE REPOSITIONING A BOEING 737-200, N11244, TO CONTINENTAL DEPARTURE GATE 41. THE LEFT SEAT MECHANIC DID NOT UTILIZE THE MECHANIC TAXI CHECKLIST. THIS MECHANIC SUBSEQUENTLY REPORTED DIFFICULTY IN NOSE WHEEL STEERING AND BRAKING. THE RIGHT SEAT MECHANIC OFFERED TO CALL MAINTENANCE; HOWEVER, THE OTHER MECHANIC DECLINED THE OFFER. AT THE TIME, FLIGHT 1176, A BOEING 737-300, N14336, FROM GATE 44 WAS UNDER CONTROL OF THE PUSHBACK TEAM. THE CREW OF THE PUSHBACK AIRPLANE AND WITNESSES REPORTED THE REPOSITIONING AIRPLANE ENGINES WERE AT 'A VERY HIGH POWER SETTING' AND 'TAXIING AT A HIGH RATE OF SPEED.' THE RIGHT WING OF AIRPLANE N11244 WAS SUBSTANTIALLY DAMAGED WHEN IT HIT THE LEFT OUTBOARD FLAP AREA OF N14336. THE HYDRAULIC SYSTEMS FOR THE NOSE WHEEL STEERING, THE MAIN WHEEL STEERING, THE MAIN WHEEL BRAKES, AND THE THRUST REVERSERS WERE FUNCTIONALLY TESTED AND FOUND OPERATIONAL.
Probable Cause: THE FAILURE OF MAINTENANCE PERSONNEL TO FOLLOW THE TAXI CHECKLIST RESULTING IN THE HYDRAULIC PUMPS NOT BEING TURNED ON.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | FTW95IA053 |
Status: | Investigation completed |
Duration: | 7 months |
Download report: | Final report |
|
Sources:
NTSB FTW95IA053
History of this aircraft
Other occurrences involving this aircraft Location
Revision history:
Date/time | Contributor | Updates |
15-Mar-2024 11:54 |
ASN Update Bot |
Added |
The Aviation Safety Network is an exclusive service provided by:
CONNECT WITH US:
©2024 Flight Safety Foundation