ASN Wikibase Occurrence # 359564
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Date: | Wednesday 16 November 1994 |
Time: | 10:45 LT |
Type: | Cessna 182P |
Owner/operator: | Double Eagle Aviation |
Registration: | N5931J |
MSN: | 18263582 |
Year of manufacture: | 1975 |
Total airframe hrs: | 2480 hours |
Engine model: | CONTINENTAL O-470-S |
Fatalities: | Fatalities: 0 / Occupants: 1 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Haskell, OK -
United States of America
|
Phase: | Initial climb |
Nature: | Ferry/positioning |
Departure airport: | |
Destination airport: | Muskogee, OK (KMKO) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:DURING TAKEOFF INITIAL CLIMB FROM RUNWAY 35, APPROXIMATELY 150 TO 200 FEET, THE ENGINE LOST POWER. A FORCED LANDING WAS MADE ON THE FIELD WEST OF THE RUNWAY. THE PILOT STATED THAT 'THE MAIN GEAR FIRST CONTACTED THE GROUND 150 FEET FROM THE WESTERN TREE LINE. BRAKING ON THE WET GRASS WAS INEFFECTIVE AND IN A MATTER OF SECONDS THE PLANE IMPACTED THE TREE LINE.' THE AIRPLANE HAD AN ANNUAL INSPECTION COMPLETED ON NOVEMBER 15, 1994, DURING WHICH BOTH FUEL CAPS AND CAP ADAPTERS HAD BEEN REPLACED. WHILE THIS MAINTENANCE WAS BEING ACCOMPLISHED, THE AIRPLANE WAS PARKED OUTSIDE OF THE HANGAR WHEN ACTUAL WORK WAS NOT BEING PERFORMED, WITH THE FUEL CAPS AND CAP ADAPTERS NOT INSTALLED. DURING PREFLIGHT OF THE AIRPLANE FOR THE FIRST FLIGHT SINCE THE ANNUAL INSPECTION, THE PILOT FOUND WATER IN FOUR FUEL SAMPLES TAKEN FROM THE FUEL STRAINER. ON THE FIFTH, SIXTH, AND SEVENTH FUEL SAMPLE TAKEN THERE WAS NO LONGER ANY EVIDENCE OF WATER. DURING THE EXAMINATION OF THE AIRPLANE AND ENGINE BY THE FAA INSPECTOR, APPROXIMATELY 4 OUNCES OF WATER WAS DRAINED FROM THE CARBURETOR BOWL AND GASCOLATOR. THE ENGINE WAS DISPLACED AND THE LEFT WING WAS DAMAGED.
Probable Cause: THE TOTAL LOSS OF ENGINE POWER DUE TO CONTAMINATED FUEL. FACTORS WERE THE IMPROPER MAINTENANCE PROCEDURES RESULTING IN FUEL CONTAMINATION, THE PILOT'S INADEQUATE PREFLIGHT INSPECTION, AND THE LACK OF SUITABLE TERRAIN AVAILABLE FOR THE FORCED LANDING.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | FTW95LA045 |
Status: | Investigation completed |
Duration: | 6 months |
Download report: | Final report |
|
Sources:
NTSB FTW95LA045
Location
Revision history:
Date/time | Contributor | Updates |
15-Mar-2024 12:13 |
ASN Update Bot |
Added |
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