ASN Wikibase Occurrence # 359882
This information is added by users of ASN. Neither ASN nor the Flight Safety Foundation are responsible for the completeness or correctness of this information.
If you feel this information is incomplete or incorrect, you can
submit corrected information.
Date: | Monday 29 August 1994 |
Time: | 12:15 LT |
Type: | Cessna 210L |
Owner/operator: | Private |
Registration: | N712JM |
MSN: | 21060432 |
Year of manufacture: | 1974 |
Total airframe hrs: | 1744 hours |
Engine model: | CONTINENTAL IO-520 |
Fatalities: | Fatalities: 0 / Occupants: 3 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Orr, MN -
United States of America
|
Phase: | Approach |
Nature: | Private |
Departure airport: | Evansville, IN (KEVV) |
Destination airport: | |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:THE PILOT REPORTED HE WAS ON FINAL APPROACH TO LAND WHEN HE 'NOTICED A SUDDEN DROP IN ALTITUDE.' HE ATTEMPTED TO INCREASE POWER, BUT THE ENGINE DID NOT RESPOND. HE SWITCHED FUEL TANKS, AND THE ENGINE STILL DID NOT RECOVER. AN EMERGENCY LANDING WAS MADE SHORT OF THE RUNWAY IN A MARSHY WET LAND WITH TALL GRASS. DURING THE LANDING, THE GEAR COLLAPSED, AND THE AIRPLANE SLID INTO A TREE STUMP AND NOSED OVER. THE PILOT AND TWO PASSENGERS EACH REPORTED THAT BOTH FUEL GAUGES WERE INDICATING 50 POUNDS AT THE TIME OF THE ACCIDENT. AN INVESTIGATION REVEALED THE FUEL SELECTOR VALVE WAS SET TO THE LEFT TANK FEED POSITION, AND THE LEFT FUEL TANK CONTAINED ONLY THREE OUNCES OF FUEL. THE RIGHT TANK CONTAINED ONLY TWO GALLONS OF FUEL. NO FUEL SPILLAGE WAS NOTED, AND THE FUEL LINE TO THE DISTRIBUTION MANIFOLD CONTAINED NO FUEL.
Probable Cause: IMPROPER PLANNING/DECISION BY THE PILOT, WHICH RESULTED IN FUEL EXHAUSTION DUE TO AN INADEQUATE SUPPLY OF FUEL. FACTORS RELATING TO THE ACCIDENT WERE: THE FALSE INDICATION FROM THE FUEL QUANTITY GAUGES, AND TERRAIN CONDITION IN THE EMERGENCY LANDING AREA.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | CHI94LA304 |
Status: | Investigation completed |
Duration: | 1 year and 2 months |
Download report: | Final report |
|
Sources:
NTSB CHI94LA304
History of this aircraft
Other occurrences involving this aircraft
17 October 2022 |
N93845 |
WYO Ventures LLC |
0 |
Hale County Airport (Plainview, TX) KPVW |
|
sub |
Location
Revision history:
Date/time | Contributor | Updates |
15-Mar-2024 15:34 |
ASN Update Bot |
Added |
The Aviation Safety Network is an exclusive service provided by:
CONNECT WITH US:
©2024 Flight Safety Foundation