ASN Wikibase Occurrence # 359887
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Date: | Sunday 28 August 1994 |
Time: | 15:10 LT |
Type: | Cessna 402 |
Owner/operator: | Private |
Registration: | N966JW |
MSN: | 402-0066 |
Year of manufacture: | 1967 |
Engine model: | CONTINENTAL TSIO-520-E |
Fatalities: | Fatalities: 0 / Occupants: 7 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Harlingen, TX -
United States of America
|
Phase: | Initial climb |
Nature: | Unknown |
Departure airport: | |
Destination airport: | (KMMA) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:FOLLOWING UNSUCCESSFUL ATTEMPTS TO START THE ENGINES, A MECHANIC REMOVED THE 'P' LEADS ON ALL MAGNETOS MAKING IT IMPOSSIBLE TO COMPLETE THE RUN-UP CHECKS. SECONDS AFTER GEAR RETRACTION THE AIRPLANE VELOCITY DECREASED AND FROM ABOUT 200 FEET MSL, A FORCED LANDING WAS MADE TO A PLOWED FIELD. PASSENGERS REPORTED HEARING THE STALL WARNING. ENGINE CONTINUITY WAS CONFIRMED. DIFFERENTIAL COMPRESSION CHECKS FOUND 4 CYLINDERS BELOW 60 PSI FOR THE LEFT AND 5 CYLINDERS BELOW 60 PSI FOR THE RIGHT. POINTS ON ALL MAGNETOS WERE BURNED AND THE LEFT MAGNETO ON EACH ENGINE WOULD NOT FIRE. ALL SPARK PLUGS EXHIBITED WEAR AND DEPOSITS IN THE ELECTRODES. BOTTOM PLUGS FROM THE LEFT ENGINE CYLINDERS #3 AND #5 WOULD NOT FIRE AND THE BOTTOM PLUGS FROM THE RIGHT ENGINE CYLINDERS #1, #3, #4, #5, AND #6 WOULD NOT FIRE. TOP PLUGS FROM THE RIGHT ENGINE CYLINDERS #5 AND #6 WOULD NOT FIRE. THE LEFT ENGINE FUEL CONTROL UNIT THROTTLE BODY WAS NOT CLAMPED AT THE TURBOCHARGER. THERE WERE 6 MALE PASSENGERS, THEIR BAGGAGE, AND 120 GALLONS OF FUEL ABOARD. DENSITY ALTITUDE WAS CALCULATED AT 2,600 FEET.
Probable Cause: THE PILOT'S FAILURE TO MAINTAIN AIRSPEED RESULTING IN AN INADVERTENT STALL. FACTORS WERE A PARTIAL LOSS OF POWER ON ALL ENGINES DUE TO WORN AND FOULED SPARK PLUGS AND INADEQUATE MAINTENANCE BY COMPANY MAINTENANCE PERSONNEL, AIRCRAFT WEIGHT BEYOND LIMITATIONS, AND HIGH DENSITY ALTITUDE.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | FTW94FA282 |
Status: | Investigation completed |
Duration: | 8 months |
Download report: | Final report |
|
Sources:
NTSB FTW94FA282
Revision history:
Date/time | Contributor | Updates |
15-Mar-2024 15:40 |
ASN Update Bot |
Added |
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