ASN Wikibase Occurrence # 360193
This information is added by users of ASN. Neither ASN nor the Flight Safety Foundation are responsible for the completeness or correctness of this information.
If you feel this information is incomplete or incorrect, you can
submit corrected information.
Date: | Saturday 9 July 1994 |
Time: | 17:09 LT |
Type: | Quickie |
Owner/operator: | Private |
Registration: | N8036W |
MSN: | 194 |
Total airframe hrs: | 383 hours |
Engine model: | ONAN B48GA018 |
Fatalities: | Fatalities: 0 / Occupants: 1 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Camarillo, CA -
United States of America
|
Phase: | Initial climb |
Nature: | Private |
Departure airport: | |
Destination airport: | |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:After takeoff on runway 26, the engine began to run rough as the aircraft reached 90 feet agl. Initially, when the pilot reduced the throttle almost to idle, the roughness dissipated. He then tried to advance the throttle, but the engine failed to develop any power. Anticipating an emergency forced landing and due to the lack of remaining runway, the pilot elected to turn toward a perpendicular taxiway. The pilot touched down in a flat open area beyond the taxiway. The left canard touched first causing the aircraft to ground loop. After an examination of the engine, the pilot concluded that a malfunction had occurred in the engine ignition system.
Probable Cause: the failure or malfunction of the engine ignition system.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | LAX94LA279 |
Status: | Investigation completed |
Duration: | 4 months |
Download report: | Final report |
|
Sources:
NTSB LAX94LA279
Location
Revision history:
Date/time | Contributor | Updates |
15-Mar-2024 18:51 |
ASN Update Bot |
Added |
The Aviation Safety Network is an exclusive service provided by:
CONNECT WITH US:
©2024 Flight Safety Foundation