ASN Wikibase Occurrence # 360527
This information is added by users of ASN. Neither ASN nor the Flight Safety Foundation are responsible for the completeness or correctness of this information.
If you feel this information is incomplete or incorrect, you can
submit corrected information.
Date: | Sunday 1 May 1994 |
Time: | 17:15 LT |
Type: | Beechcraft K35 Bonanza |
Owner/operator: | Private |
Registration: | N441B |
MSN: | D-5943 |
Year of manufacture: | 1959 |
Fatalities: | Fatalities: 0 / Occupants: 2 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Gustavus, AK -
United States of America
|
Phase: | En route |
Nature: | Private |
Departure airport: | Juneau, AK (JNU) |
Destination airport: | |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:THE PILOT SWITCHED FROM HIS AUXILIARY FUEL TANK TO HIS LEFT MAIN FUEL TANK WHEN THE ENGINE STOPPED PRODUCING POWER. HE HAD TO DITCH IN THE BAY. THE PILOT SAID HE THOUGHT THE ENGINE FAILED DUE TO FUEL MISMANAGEMENT.
Probable Cause: THE PILOT-IN-COMMAND'S DELAY IN SELECTING THE MAIN FUEL TANK POSITION. THE LACK OF SUITABLE TERRAIN FOR A FORCED LANDING WAS A FACTOR.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | ANC94LA053 |
Status: | Investigation completed |
Duration: | 9 months |
Download report: | Final report |
|
Sources:
NTSB ANC94LA053
History of this aircraft
Other occurrences involving this aircraft Location
Revision history:
Date/time | Contributor | Updates |
16-Mar-2024 08:21 |
ASN Update Bot |
Added |
The Aviation Safety Network is an exclusive service provided by:
CONNECT WITH US:
©2024 Flight Safety Foundation