ASN Wikibase Occurrence # 360639
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Date: | Monday 4 April 1994 |
Time: | 11:40 LT |
Type: | Talago THUNDERGULL JT2 |
Owner/operator: | Stanley Talago |
Registration: | N73ST |
MSN: | ST3503 |
Total airframe hrs: | 8 hours |
Engine model: | ROTAX 912-WL |
Fatalities: | Fatalities: 0 / Occupants: 1 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Clarksburg, WV -
United States of America
|
Phase: | Initial climb |
Nature: | Private |
Departure airport: | (KCKB) |
Destination airport: | |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:THE AIRPLANE HAD JUST TAKEN OFF AND WAS IN ITS INITIAL CLIMB WHEN CONTROL WAS LOST. THE AIRPLANE COLLIDED WITH TERRAIN IN AN UNCONTROLLED DESCENT. THE PILOT STATED, 'AFTER A GOOD PRE-FLIGHT THE TOWER CLEARED ME TO DEPART...IMMEDIATELY ON LIFT OFF, THE AIRCRAFT JUMPED TO THE RIGHT. THERE WAS DEFINITELY A CONTROL PROBLEM BUT I HAVE NOT PINPOINTED WHERE.' THE FAA INSPECTOR'S POST ACCIDENT EXAMINATION REVEALED THE BOLT CONNECTING THE TWO RODS IN THE AILERON PUSH/PULL ROD ASSEMBLY WAS MISSING. THE BOLT HOLES IN BOTH RODS SHOWED NO DEFORMATION. ADDITIONALLY, THIS BOLT WAS CONNECTED WITH THE JAM NUT FOUND LOOSE DURING THE CONFORMITY INSPECTION. THE AIRPLANE HAD A TOTAL OF 4 HOURS. A CONFORMITY INSPECTION WAS PERFORMED BY AN FAA DESIGNATED AIRWORTHINESS REPRESENTATIVE (DAR) ON NOVEMBER 29, 1993. THE DAR'S CONFORMITY INSPECTION REPORT STATED 'JAM NUT LOOSE ON AILERON CONTROL IN OVERHEAD.' THE REPORT REVEALED THAT THE CORRECTIVE ACTION TAKEN WAS THAT THE BOLT WAS 'TIGHTENED.' THE KIT MANUFACTURER SPECIFIES THE USE OF A SELF LOCKING NUT, HOWEVER, THE PILOT USED A JAM NUT.
Probable Cause: The builder's inadequate maintenance adjustment which resulted in the aileron control assembly becoming disconnected.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | BFO94LA060 |
Status: | Investigation completed |
Duration: | 1 year and 6 months |
Download report: | Final report |
|
Sources:
NTSB BFO94LA060
Location
Revision history:
Date/time | Contributor | Updates |
16-Mar-2024 09:33 |
ASN Update Bot |
Added |
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