This information is added by users of ASN. Neither ASN nor the Flight Safety Foundation are responsible for the completeness or correctness of this information.
If you feel this information is incomplete or incorrect, you can
submit corrected information.
Date: | Tuesday 1 March 1994 |
Time: | 01:05 LT |
Type: | Lockheed L-1011 TriStar 1 |
Owner/operator: | Rich International Airways |
Registration: | N303EA |
MSN: | 193A-1004 |
Total airframe hrs: | 46234 hours |
Engine model: | Rolls-Royce RB-211-22B |
Fatalities: | Fatalities: 0 / Occupants: 14 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Fairbanks, AK -
United States of America
|
Phase: | Take off |
Nature: | Unknown |
Departure airport: | (KFAI) |
Destination airport: | Miami, FL (KMIA) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:AS FULL POWER WAS APPLIED FOR TAKEOFF, THERE WAS A RUPTURE OF THE 6TH STAGE DISC ON THE INTERMEDIATE COMPRESSOR 6/7TH ROTOR SHAFT ASSEMBLY IN THE #3 ENGINE. PIECES OF DISC SEVERED A FUEL INLET LINE & PENETRATED THE #1 ENGINE & THE FUSELAGE. FIRE WARNINGS FOR THE #3 & #1 ENGINES WERE ACTIVATED & ENGINE FIRE BOTTLES WERE DISCHARGED DURING AN ABORTED TAKEOFF. RESIDUAL FIRE IN ONE ENGINE WAS EXTINGUISHED BY AIRPORT FIRE FIGHTERS. ABOUT 80% OF THE FAILED DISC WAS FOUND; METALLURGICAL EXAMINATION SHOWED CORROSION PITTING & SMALL FATIGUE CRACKS AT THE ATTACHMENT HOLES. THE LARGEST CRACK WAS 0.13' DEEP & 0.23' WIDE. ACCORDING TO ROLLS ROYCE CALCULATIONS, THIS SIZE CRACK WOULD NOT HAVE RESULTED IN FAILURE UNLESS THE N2 ROTOR RPM HAD REACHED 118%. A TELLTALE MARKER FOR THE FLIGHT ENGINEER'S #3 N2 GAUGE SHOWED 106% (RED-LINE WAS 102.5%), BUT THE TELLTALE MARKER WAS OUT OF CALIBRATION; THEREFORE, OVERSPEED WAS NOT VERIFIED. MAX EPR FOR TAKEOFF WAS WITHIN LIMITS. SERVICE BULLETIN (SB) RB.211-72-9569 REQUIRED THAT ROTORS EXCEEDING 14,000 CYCLES BE REMOVED BY 4/30/93; THE FAILED ROTOR HAD 16,327 CYCLES. THE SB WAS 'S-MANDATORY' IN THE U.K., BUT IT WAS NOT MANDATORY IN THE U.S.
Probable Cause: FAILURE OF THE SIXTH STAGE DISC ON THE INTERMEDIATE COMPRESSOR STAGE 6/7TH ROTOR SHAFT ASSEMBLY IN THE NUMBER THREE ENGINE, DUE TO CORROSION PITTING AND FATIGUE CRACKING OF THE FAILED DISC. A FACTOR RELATED TO THE ACCIDENT WAS: FAILURE OF THE AIRLINE COMPANY TO FOLLOW PROVISIONS OF THE SERVICE BULLETIN. FOREIGN OBJECT DAMAGE TO THE NUMBER ONE ENGINE WAS THE RESULT OF THE UNCONTAINED FAILURE OF THE NUMBER THREE ENGINE.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | ANC94FA036 |
Status: | Investigation completed |
Duration: | 1 year and 3 months |
Download report: | Final report |
|
Sources:
NTSB ANC94FA036
Location
Revision history:
Date/time | Contributor | Updates |
16-Mar-2024 11:11 |
ASN Update Bot |
Added |
The Aviation Safety Network is an exclusive service provided by:
CONNECT WITH US:
©2024 Flight Safety Foundation