Accident Lockheed L-1011 TriStar 1 N303EA,
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Date:Tuesday 1 March 1994
Time:01:05 LT
Type:Silhouette image of generic L101 model; specific model in this crash may look slightly different    
Lockheed L-1011 TriStar 1
Owner/operator:Rich International Airways
Registration: N303EA
MSN: 193A-1004
Total airframe hrs:46234 hours
Engine model:Rolls-Royce RB-211-22B
Fatalities:Fatalities: 0 / Occupants: 14
Aircraft damage: Substantial
Category:Accident
Location:Fairbanks, AK -   United States of America
Phase: Take off
Nature:Unknown
Departure airport:(KFAI)
Destination airport:Miami, FL (KMIA)
Investigating agency: NTSB
Confidence Rating: Accident investigation report completed and information captured
Narrative:
AS FULL POWER WAS APPLIED FOR TAKEOFF, THERE WAS A RUPTURE OF THE 6TH STAGE DISC ON THE INTERMEDIATE COMPRESSOR 6/7TH ROTOR SHAFT ASSEMBLY IN THE #3 ENGINE. PIECES OF DISC SEVERED A FUEL INLET LINE & PENETRATED THE #1 ENGINE & THE FUSELAGE. FIRE WARNINGS FOR THE #3 & #1 ENGINES WERE ACTIVATED & ENGINE FIRE BOTTLES WERE DISCHARGED DURING AN ABORTED TAKEOFF. RESIDUAL FIRE IN ONE ENGINE WAS EXTINGUISHED BY AIRPORT FIRE FIGHTERS. ABOUT 80% OF THE FAILED DISC WAS FOUND; METALLURGICAL EXAMINATION SHOWED CORROSION PITTING & SMALL FATIGUE CRACKS AT THE ATTACHMENT HOLES. THE LARGEST CRACK WAS 0.13' DEEP & 0.23' WIDE. ACCORDING TO ROLLS ROYCE CALCULATIONS, THIS SIZE CRACK WOULD NOT HAVE RESULTED IN FAILURE UNLESS THE N2 ROTOR RPM HAD REACHED 118%. A TELLTALE MARKER FOR THE FLIGHT ENGINEER'S #3 N2 GAUGE SHOWED 106% (RED-LINE WAS 102.5%), BUT THE TELLTALE MARKER WAS OUT OF CALIBRATION; THEREFORE, OVERSPEED WAS NOT VERIFIED. MAX EPR FOR TAKEOFF WAS WITHIN LIMITS. SERVICE BULLETIN (SB) RB.211-72-9569 REQUIRED THAT ROTORS EXCEEDING 14,000 CYCLES BE REMOVED BY 4/30/93; THE FAILED ROTOR HAD 16,327 CYCLES. THE SB WAS 'S-MANDATORY' IN THE U.K., BUT IT WAS NOT MANDATORY IN THE U.S.

Probable Cause: FAILURE OF THE SIXTH STAGE DISC ON THE INTERMEDIATE COMPRESSOR STAGE 6/7TH ROTOR SHAFT ASSEMBLY IN THE NUMBER THREE ENGINE, DUE TO CORROSION PITTING AND FATIGUE CRACKING OF THE FAILED DISC. A FACTOR RELATED TO THE ACCIDENT WAS: FAILURE OF THE AIRLINE COMPANY TO FOLLOW PROVISIONS OF THE SERVICE BULLETIN. FOREIGN OBJECT DAMAGE TO THE NUMBER ONE ENGINE WAS THE RESULT OF THE UNCONTAINED FAILURE OF THE NUMBER THREE ENGINE.

Accident investigation:
cover
  
Investigating agency: NTSB
Report number: ANC94FA036
Status: Investigation completed
Duration: 1 year and 3 months
Download report: Final report

Sources:

NTSB ANC94FA036

Location

Revision history:

Date/timeContributorUpdates
16-Mar-2024 11:11 ASN Update Bot Added

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