ASN Wikibase Occurrence # 360831
This information is added by users of ASN. Neither ASN nor the Flight Safety Foundation are responsible for the completeness or correctness of this information.
If you feel this information is incomplete or incorrect, you can
submit corrected information.
Date: | Wednesday 16 February 1994 |
Time: | 11:20 LT |
Type: | Cessna 172N |
Owner/operator: | Private |
Registration: | N737ZY |
MSN: | 17269813 |
Year of manufacture: | 1977 |
Total airframe hrs: | 4416 hours |
Engine model: | LYCOMING O-320-H2AD |
Fatalities: | Fatalities: 0 / Occupants: 2 |
Aircraft damage: | Substantial |
Category: | Accident |
Location: | Georgetown, AR -
United States of America
|
Phase: | En route |
Nature: | Private |
Departure airport: | Marked Tree, AR (6M8 |
Destination airport: | Searcy, AR (M07) |
Investigating agency: | NTSB |
Confidence Rating: | Accident investigation report completed and information captured |
Narrative:THE PILOT STATED THAT AFTER CIRCLING A TOWN SEVERAL TIMES WHILE ATTEMPTING TO FIND A PRIVATE AIR STRIP, HE DECIDED TO FLY TO A NEARBY AIRPORT. SHORTLY THEREAFTER THE ENGINE BEGAN RUNNING ROUGH AND LOSING RPM. THE PILOT'S EFFORTS TO REGAIN POWER WERE UNSUCCESSFUL AND THE AIRPLANE WOULD NOT SUSTAIN LEVEL FLIGHT. HE ELECTED TO EXECUTE A FORCED LANDING ON A GRAVEL ROAD. TOUCHDOWN WAS SUCCESSFUL; HOWEVER, AFTER A SHORT GROUND ROLL, THE PILOT LIFTED THE AIRPLANE OFF AGAIN TO AVOID HITTING A HIGH TREE STUMP. AFTER TOUCHING DOWN THE SECOND TIME THE LEFT WING STRUCK A TELEPHONE POLE AND THE AIRPLANE YAWED INTO A DITCH. THE ICING PROBABILITY CHARTS INDICATED THE POTENTIAL FOR SERIOUS ICING EXISTED AT CRUISE POWER FOR THE ATMOSPHERIC CONDITIONS THAT WERE PRESENT. TEMPERATURE AND DEW POINT WERE 48 AND 35 DEGREES F, RESPECTIVELY.
Probable Cause: A CARBURETOR ICING INDUCED POWER LOSS DUE TO THE PILOT'S IMPROPER USE OF CARBURETOR HEAT IN CONDITIONS CONDUCIVE TO CARBURETOR ICING. A FACTOR WAS THE LACK OF SUITABLE TERRAIN ONTO WHICH A FORCED LANDING COULD BE EXECUTED.
Accident investigation:
|
| |
Investigating agency: | NTSB |
Report number: | FTW94LA083 |
Status: | Investigation completed |
Duration: | 9 months |
Download report: | Final report |
|
Sources:
NTSB FTW94LA083
Revision history:
Date/time | Contributor | Updates |
16-Mar-2024 11:37 |
ASN Update Bot |
Added |
The Aviation Safety Network is an exclusive service provided by:
CONNECT WITH US:
©2024 Flight Safety Foundation